jul-aug2012
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Flight Safety Australia<br />
Issue 87 July–August 2012<br />
37<br />
SELECTED SERVICE DIFFICULTY REPORTS ... CONT.<br />
Cessna TR182 Elevator cable frayed.<br />
SDR 510014722 (photo below)<br />
Broken strands in elevator trim cable.<br />
P/No: 0510105248. TSN: 967 hours.<br />
Socata TB10TOBAGO Wing spar cracked.<br />
SDR 510014561 (photo below)<br />
LH and RH forward wing attachment small spars<br />
cracked in area adjacent to lower inboard bolt.<br />
Fifteen similar reports submitted for this type of<br />
aircraft in reporting period. P/No: TB1011000101.<br />
TSN: 11,893 hours.<br />
Cessna U206F Landing gear attach fitting<br />
cracked. SDR 510014797 (photo below)<br />
LH main landing gear attachment fitting cracked.<br />
P/No: 1211601497. TSN: 8,766 hours.<br />
Cessna U206G Power lever cable binding.<br />
SDR 510014643<br />
Engine throttle cable binding. Cable was an almost<br />
new item with only 37 hours TSN.<br />
P/No: 986305313. TSN: 37 hours/1 month.<br />
Giplnd GA200C Wing spar cracked.<br />
SDR 510014765 (photo below)<br />
Wing front lower spar cap cracked in area between<br />
WS 0.00 and WS 4.50 in area of wing/fuselage<br />
attachment. Crack length approximately 114.3mm<br />
(4.5in). Found during inspection iaw SB GA200-<br />
2011-06 Issue1. Aircraft registered in New Zealand.<br />
P/No: GA2005710025.<br />
Giplnd GA8 Horizontal stabiliser spar cap<br />
cracked. SDR 510014800 (photo below)<br />
Horizontal stabiliser rear lower spar cap cracked.<br />
Found during inspection iaw SB GA8-2002-02<br />
Issue 6. P/No: GA855102115<br />
Giplnd GA8 Trailing edge fitting rusted.<br />
SDR 510014723 (photo following)<br />
LH and RH trailing edge flap torque tube outboard<br />
fittings corroded (rusted).<br />
P/No: GA82750121413. TSN: 3,072 hours.<br />
Gulfstream 500S Hydraulic tube corroded.<br />
SDR 510014540<br />
Rigid hydraulic tubing located between LH wing<br />
root and engine nacelle contained corrosion pitting<br />
through wall thickness resulting in loss of hydraulic<br />
fluid. Suspect caused by tubing contacting flexible<br />
hose in wing channel. P/No: 5052038.<br />
Gulfstream 500S Landing gear retract/extend<br />
system bolt failed. SDR 510014538<br />
Landing gear uplock pivot bolt failed in area<br />
covered by bearing inner face. Investigation indicates<br />
failure might have been propagating for some time.<br />
P/No: AN174C21A.<br />
Piper PA24 Horizontal stabiliser fitting cracked.<br />
SDR 510014796 (photo below)<br />
Stabiliser horn balance attachment cracked<br />
from stabiliser attachment holes to balance tube<br />
attachment. TSN: 2,679 hours.<br />
Piper PA32R301T Fuselage door sill corroded.<br />
SDR 510014593 (photo below)<br />
Rear cabin door had localised corrosion at screw<br />
holes. Interior upholstery stainless steel screws and<br />
moisture in upholstery contributed to the corrosion.<br />
P/No: 68334000. TSN: 1,372 hours/144 months.<br />
Piper PA44180 Emergency exit separated.<br />
SDR 510014704<br />
Emergency exit/window forward latch disengaged<br />
allowing airflow, causing window and frame<br />
to separate from fuselage. P/No: 8660202.<br />
TSN: 8,590 hours.<br />
Piper PA60601B Cabin door opened.<br />
SDR 510014767<br />
Top half of main cabin door opened following<br />
take-off. Investigation found no faults with the door<br />
and no structural damage.<br />
Swrngn SA227AC Nose landing gear shimmy.<br />
SDR 510014577 (photo below)<br />
Nose landing gear shimmy on landing. Initial<br />
investigation found broken bolts at the NLG<br />
steering actuator. P/No: 2752500001. TSN: 30,174<br />
hours/45,110 cycles.<br />
Swrngn SA227DC Brake leaking.<br />
SDR 510014761<br />
RH outboard brake unit leaking and tyre deflated.<br />
Loss of hydraulic fluid.<br />
Swrngn SA227DC Landing gear faulty.<br />
SDR 510014764<br />
Pilots felt a repetitive bump and noticed the hydraulic<br />
pressure fluctuating during landing gear retraction.<br />
Landing gear suspect faulty. Investigation continuing.<br />
TSN: 20,006 hours/22,141 cycles.<br />
Components<br />
Fuel injection system suspect unapproved part.<br />
SDR 510014803<br />
RSA and Silver Hawk EX fuel injection system may be<br />
suspect/counterfeit parts. Precision Airmotive are the<br />
only manufacturer and distributor of these systems.<br />
Balloon cable worn. SDR 510014545<br />
(photo below)<br />
Hot air balloon basket suspension cables worn in<br />
area of contact with burner frame nylon support pole.<br />
TSN: 1,981 hours/138 months.<br />
Balloon load frame cracked. SDR 510013682<br />
Balloon burner load frame had several hairline cracks<br />
along original welds.<br />
P/No: KLF201088. TSN: 1,423 hours/123 months.