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The ITER toroidal field model coil project

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210 A. Ulbricht et al. / Fusion Engineering and Design 73 (2005) 189–327<br />

<strong>The</strong> smooth and safe cool down, as shown in this<br />

Fig. 4.4, was limited by the thermal conduction not<br />

by the refrigerator cooling capacity.<br />

All components were cooled in parallel with the<br />

mass flow rate coming directly from the 2 kW refrigerator.<br />

<strong>The</strong> mass flow rates of the individual components<br />

were adjusted manually in order to minimize the temperature<br />

differences in the test arrangement. <strong>The</strong> total<br />

mass flow rate was in the range between 75 and 95 g/s.<br />

At the start of the cool down the cooling power was<br />

around 7 kW and decreased at the end to 2 kW. <strong>The</strong> cool<br />

down was stopped for 6 h at 77 K as shown in Fig. 4.4<br />

for a calibration of the current distribution measurement.<br />

<strong>The</strong> vacuum pressure in B300 was 9 × 10 −4 mbar<br />

at room temperature and reached 5.6 × 10 −6 mbar at<br />

LHe Temperature. During the cool down, and also during<br />

operation, the leak rate was checked frequently<br />

and no indication of a significant leak was found (see<br />

Table 4.2).<br />

<strong>The</strong> warm up was also computer-controlled above<br />

20 K, like the cool down, and the time needed was 2<br />

weeks in both test phases.<br />

4.3.2. Cryogenic operation<br />

<strong>The</strong> control dewar B250 was filled with LHe in<br />

parallel at the end of the cool down. When the cool<br />

Fig. 4.4. Cool down of the TFMC test configuration for test Phase 2.<br />

down was finished the secondary cooling loop was<br />

pressurised to supercritical conditions. By means of the<br />

He piston pumps, the supercritical He was then circulated<br />

in the cooling loop of the <strong>coil</strong>s. For the extended<br />

operation with a required mass flow rate up to 280 g/s,<br />

both piston pumps were operated in parallel. <strong>The</strong> mass<br />

flow rate of the different components was adjusted to<br />

the values as listed in Table 4.4. Also the heat load<br />

of the various components was investigated carefully<br />

before current operation and the results are included in<br />

Table 4.4 as standby values. <strong>The</strong> measured values were<br />

in good agreement with the calculated ones except of<br />

the heat load of the bus bars types 1 and 2. This heat<br />

load of 36 W for the negative and 40 W for the positive<br />

bus bar required a high He mass flow rate in order<br />

to keep the outlet temperature of the bus bars below<br />

6 K and avoid a quench of the NbTi conductor during<br />

current operation. <strong>The</strong> reason for this unexpected high<br />

heat load could not be clarified up to now.<br />

An advantage of the conductor and TFMC winding<br />

design is the relatively low pressure drop that was<br />

measured at room temperature as well as at LHe temperature<br />

(see Section 6.2.1) [51] and the relatively<br />

uniform mass flow distribution in the TFMC winding<br />

without an active control as shown in Fig. 4.5. <strong>The</strong> maximum<br />

deviation from the average mass flow rate was<br />

around −10% in DP4 and around +10% in DP5. <strong>The</strong>se

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