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English Edition (6 MB pdf) - Saudi Aramco

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needed a fit-for-purpose bit design to match the system and to<br />

increase the steerability and stability, which were the weak<br />

points indentified in the first run with the PRSS. The first step<br />

included an in-depth analysis of Bit A to identify its strengths<br />

and weaknesses, and to establish an action plan for the next<br />

iteration. Among the strong points, it was clear that the use of<br />

eight blades and 19 mm cutters as the primary cutting<br />

structure provided a good balance between bit life and ROP;<br />

consequently, it was decided to continue with this geometry.<br />

Bit A recorded several vibration incidents, with slip-stick<br />

recorded at the surface and measured while drilling (MWD)<br />

shocks registered by the downhole tools. The cutters exhibited<br />

medium wear, and several chipped cutters indicated a need for<br />

improvements in the cutting structure. The force imbalance<br />

values, which were one of the few analytical components<br />

initially available when Bit B was designed, showed relatively<br />

high values. The ideal bit force imbalance scenario occurs<br />

when the values are near zero; values of less than 4% are<br />

accepted as the minimum standard.<br />

The cutting structure of the new Bit B included few<br />

changes, as compared with Bit A. To gain stability and<br />

improve the force imbalance values, the angle of the back<br />

rakes was adjusted by 15% to decrease the aggressiveness,<br />

and the blades were moved to obtain better figures. The 13<br />

mm cutters were eliminated in the bit face to increase the<br />

ROP, and the gauge length was reduced to 2½” to improve<br />

the steerability, particularly because planned future wells<br />

would require a greater BUR than the first two runs in the<br />

Haradh field. Rather than a straight gauge pad, Bit B used a<br />

spiral gauge, which considerably increased the borehole<br />

contact, Fig. 12.<br />

The cutter type in Bit B was updated to the Z3 ® cutter,<br />

which provided additional impact resistance. All force<br />

imbalance values were improved by up to 50%.<br />

Bit B was used in the next four wells, including two wells in<br />

the Haradh zone and two in the ‘Uthmaniyah zone. The 12”<br />

section in the ‘Uthmaniyah wells required building the angle<br />

from the vertical up to 74°, which tested the system’s<br />

steerability. In the first three wells of this batch, the 12”<br />

directional section was completed with one bit, but because of<br />

a long directional section in the last ‘Uthmaniyah well, the<br />

ROP became too low before the interval was completed,<br />

requiring the bit to be pulled out of the hole and the use of<br />

one more bit to complete the interval. Bit B showed better<br />

stability than Bit A; the steerability was good but not<br />

optimum because the PRSS had to be set at the maximum<br />

deflection in some intervals to achieve the required doglegs.<br />

The bit came out of the hole with a great deal of cutter wear,<br />

which explained the reduction in ROP that required the bit to<br />

be pulled out of the hole, Fig. 13.<br />

The Z3 cutter could not drill sections of more than 2,500 ft<br />

long because of the abrasiveness of the Khuff formation in the<br />

‘Uthmaniyah zone. This was the first well with such a long<br />

section, and it set a new challenge to be overcome.<br />

Fig. 12. Straight gauge pad vs. spiral gauge pad.<br />

Fig. 13. Bit B condition after drilling in the ‘Uthmaniyah zone.<br />

SAUDI ARAMCO JOURNAL OF TECHNOLOGY SUMMER 2010 51

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