Troels Dyhr Pedersen.indd - Solid Mechanics
Troels Dyhr Pedersen.indd - Solid Mechanics
Troels Dyhr Pedersen.indd - Solid Mechanics
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would not be increasing the pressure. Additionally it was argued that it would make more sense to compare<br />
HCCI data with DI CI data on the same engine if the setup was identical. The turbocharger did however<br />
increase the absolute pressure up to 1.2 bars at 1800 RPM as the total equivalence ratio was increased with<br />
methanol, which meant that the equivalence ratio for DME became lower than the target.<br />
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Engine ISUZU 4HG1T<br />
No. of cylinders 4<br />
Bore x Stroke 115 mm x 110 mm<br />
Connecting rod length 250 mm<br />
Displacement 4.57 L<br />
Compression ratio 14.5 (19.0 original)<br />
Injection system DME Common rail<br />
Rated power 88 kW @ 3000 RPM<br />
Rated torque 322 Nm @ 1800 RPM<br />
Table 1: Engine specifications<br />
The engine was coupled with a speed regulated motor-generator equipped with a load cell for measuring torque,<br />
which was used for calculating BMEP. The cylinder pressure was measured on all 4 cylinders with piezoelectric<br />
pressure pickups and logged in intervals of 1 CAD.<br />
The geometric compression ratio was reduced from 18 to 14.5 by enlarging the piston bowls. The bowl<br />
geometry was maintained to enable normal DI CI operation.<br />
Changing the engine to HCCI operation required that the electrical connections for the common rail injector<br />
were switched pair wise, due to a limited advance setting in the injector driver software. The injectors were then<br />
set to inject at the beginning of the intake stroke, since this should result in good mixing. The emission values<br />
did not indicate leakage of DME through the exhaust valves when this injection timing was used.<br />
METHANOL INJECTION SYSTEM<br />
Four low pressure gasoline injectors were installed in a custom inlet manifold. The methanol was supplied from<br />
a tank that was pressurized to three Bar. Injector drivers enabled accurate control of the injection duration and<br />
timing. The injection was adjusted to begin at inlet valve opening. Varying the timing showed no significant<br />
change to the heat release or emissions, so it was kept at this position throughout the test.<br />
TEST CONDITIONS<br />
Prior to all tests the engine was heated in normal DI CI operation with DME. After 30 minutes of preheating the<br />
engine was stopped and the injector leads were switched to inject at 360 BTDC for HCCI operation.<br />
The tests were performed at engine speeds of 1000 and 1800 RPM. These two engine speeds used were chosen<br />
since part load operation usually implies running at lower engine speeds. It is however fully possible to operate<br />
with DME HCCI combustion at higher engine speeds, such as 3000 RPM.