Troels Dyhr Pedersen.indd - Solid Mechanics
Troels Dyhr Pedersen.indd - Solid Mechanics
Troels Dyhr Pedersen.indd - Solid Mechanics
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8 Description of experimental engine setup<br />
8.1 Engine<br />
The engine used for the experimental work at DTU is a 0.9 L, 2 cylinder, 4 stroke DI CI<br />
engine which is constructed for marine applications. It is a simple construction with<br />
pushrod valve operation which makes it easy to dismantle and reassemble. The cylinder<br />
head is a flat 2 valve design. It is naturally aspirated and does not have EGR.<br />
The engine used for experiments at NTSEL in Tokyo was an Isuzu 4.6 L 4 cylinder truck<br />
engine, which was modified with a common rail system developed for DME. It was<br />
equipped with EGR and a high capacity EGR cooler. It was furthermore fitted with an<br />
injection system for methanol for the experiment. The engine and the experimental setup<br />
are described separately in the second paper in appendix.<br />
8.1.1 Engine setup<br />
The engine is coupled to an eddy current type dynamometer from Zöllner. The<br />
dynamometer does not have motoring capability, so one of the two cylinders on the<br />
engine was kept in DI CI operation with diesel fuel, in order to maintain the engine speed<br />
and heat up the engine.<br />
Figure 1: Engine stand<br />
8.1.2 Modifications<br />
The first modification needed to run the engine in HCCI mode was to adapt the<br />
compression ratio to suit the fuel ignition properties. Since the compression ratio needed<br />
to run on DME was not known initially, a solution which allowed a variable compression<br />
volume was installed in the cylinder head. The original diesel injector hole was enlarged<br />
to accommodate a steel cylinder, so that a piston could be used to control the<br />
compression volume. The arrangement is shown in figures 2 and 3. By adjusting the<br />
piston crown height a compression ratio of 14 was made, and with the adjustment piston<br />
in bottom position, the compression ratio could be varied from 9 to 14 while the engine<br />
was running. This modification has also been used in an HCCI engine at Lund University<br />
[17].