industry and environment - DTIE
industry and environment - DTIE
industry and environment - DTIE
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Chemicals management<br />
gases such as chlorine, sulphur dioxide <strong>and</strong> trioxide,<br />
nitrogen oxides, <strong>and</strong> fumes of acid <strong>and</strong> organic<br />
solvents. Much of the time, these by-products of<br />
unit processes are recovered subject to the cost of<br />
recovery <strong>and</strong> their market potential. They are normally<br />
gases like SO 2 , HCl (hydrochloric acid, or<br />
hydrogen chloride) <strong>and</strong> organic products. If they<br />
are not recovered, they cause air pollution. A 100%<br />
recovery rate is not possible; the unrecovered product<br />
is vented from the stack.<br />
Particulate matter emissions from the drying<br />
<strong>and</strong> grinding operation are another source of pollution.<br />
Concentrations can be as high as 500-600<br />
mg/litre. Flue gas from the boiler is also a source of<br />
air pollution in this sector. Very high particulate<br />
matter emissions of the dyestuff in powder form<br />
are a major source of air pollution from the<br />
dyestuff production plant.<br />
An emission st<strong>and</strong>ard exists for most types of<br />
gases <strong>and</strong> particulate matter (e.g. 50 mg/litre in<br />
the case of particulate matter).<br />
Management of gaseous emissions<br />
To meet emission limits, gases <strong>and</strong> fumes emitted<br />
from the stack are generally scrubbed using<br />
packed bed type scrubbers. Most SMEs in this<br />
sector are unable to comply with the st<strong>and</strong>ards for<br />
source or fugitive emissions.<br />
Cleaner production in the chemical<br />
<strong>industry</strong> (dye, dye intermediates<br />
<strong>and</strong> pharmaceuticals)<br />
Significant <strong>environment</strong>al degradation has<br />
occurred in various parts of India due to rapid<br />
development/industrialization. Greater <strong>environment</strong>al<br />
awareness <strong>and</strong> activism in all quarters,<br />
accompanied by the economic liberalization promoted<br />
by the Indian government, have left Indian<br />
SMEs struggling for survival. In the past decade<br />
they have experienced a financial crunch at the<br />
same time as growing pressure to improve their<br />
<strong>environment</strong>al performance. End-of-pipe treatment<br />
of waste <strong>and</strong> emissions is being promoted,<br />
but with only limited success since it is cost-intensive.<br />
And changing the form of the waste is not the<br />
same thing as eliminating it. Over the decade only<br />
a few cleaner production initiatives have been<br />
undertaken, mostly as demonstration projects. A<br />
few of these are briefly described below.<br />
A cleaner production demonstration project<br />
was carried out in 12 chemical plants in 2001-02<br />
by the National Productivity Council, located at<br />
Vapi, Gujarat. Participants were from the dye, dye<br />
intermediates <strong>and</strong> pharmaceutical sectors. During<br />
the project 788 cleaner production measures were<br />
identified. By the end of 2002, 380 had been<br />
implemented.<br />
Implementing these measures required an<br />
investment of Rs. 8.5 million. This investment is<br />
expected to yield Rs. 40 million per year through<br />
improved productivity <strong>and</strong> reduced <strong>environment</strong>al<br />
load. The measures implemented include:<br />
◆ use of purer grade naphthalene <strong>and</strong> of iron powder<br />
having higher activity, leading to an annual net<br />
saving of Rs. 0.18 million in addition to a 50%<br />
reduction of organics in sludge;<br />
◆ substitution of inorganic for organic acid in<br />
UNEP’s definition of cleaner production<br />
the final isolation of NMJ (a dye intermediate)<br />
following purification, leading to an annual<br />
net saving of Rs. 4.3 million <strong>and</strong> a 50% reduction<br />
of effluent organic load;<br />
◆ modification of acetonyl sulphonyl chloride<br />
(ASC) cake washing (static material water<br />
seeping through, changed to continuous stirring<br />
of material while washing), leading to a<br />
reduction of water <strong>and</strong> caustic consumption<br />
<strong>and</strong> improved quality of ASC. This measure<br />
produced economic savings of Rs. 6.6 million<br />
per year for an investment of Rs. 10,000;<br />
◆ increasing the height of the distillation column,<br />
leading to improved recovery of isopropyl<br />
alcohol at a bulk drug manufacturing<br />
unit. This measure produced an annual net<br />
saving of Rs. 0.8 million for an investment of<br />
Rs. 0.38 million.<br />
Ishan Dye Chem Ltd. (copper phthalo<br />
cyanine dye intermediate manufacturer)<br />
M/s Ishan Dye Chem Ltd. is a small-scale dye<br />
intermediate unit that manufactures copper<br />
phthalo cyanine (CPC), which is further<br />
processed to produce alpha <strong>and</strong> beta blue dyes.<br />
The unit produces 100 tonnes of CPC per<br />
month. A cleaner production process was introduced<br />
in order to reduce water consumption,<br />
recover solvent effectively <strong>and</strong> conserve energy.<br />
Major CP measures implemented are:<br />
◆ installation of a rotary air lock in a raw material<br />
feeding hopper to reduce solvent losses in<br />
the work atmosphere. This measure resulted in<br />
annual net savings of Rs. 1.8 million for an<br />
investment of Rs. 0.1 million;<br />
◆ increasing vacuum pressure from 400 to 700<br />
mm Hg for improved recovery of trichlorobenzene<br />
(TCB) from the heated mass in the vannulator.<br />
This measure, which required an<br />
investment of Rs. 0.5 million, led to annual net<br />
savings of Rs. 1.3 million.<br />
Metrochem Industries Ltd., Ahmedabad<br />
(H-acid dye intermediate manufacturer)<br />
M/s. Metrochem Industries Ltd. is a dye intermediate<br />
manufacturing <strong>industry</strong> with a production<br />
capacity of about 60 tonnes of H-acid (an important<br />
dye intermediate produced from naphthalene)<br />
per month. During the CP project 27 cleaner<br />
production measures were identified, of which 12<br />
were implemented. The unit invested Rs. 2.8 million<br />
in implementing the CP measures. Annual<br />
Cleaner production is the continuous application<br />
of an integrated preventive <strong>environment</strong>al<br />
strategy to processes, products <strong>and</strong> services to<br />
increase overall efficiency, <strong>and</strong> to reduce risks to<br />
humans <strong>and</strong> the <strong>environment</strong>. Cleaner production<br />
can be applied to the processes used in any<br />
<strong>industry</strong>, to products themselves, <strong>and</strong> to various<br />
services provided to society.<br />
For the production process, CP results from<br />
one or a combination of conserving raw materials,<br />
water <strong>and</strong> energy; eliminating toxic <strong>and</strong> dangerous<br />
raw materials; <strong>and</strong> reducing the quantity<br />
<strong>and</strong> toxicity of all emissions <strong>and</strong> wastes at source<br />
during the production process.<br />
For products, CP aims to reduce the <strong>environment</strong>al,<br />
health <strong>and</strong> safety impacts of products<br />
over their entire life cycles, from raw materials<br />
extraction, through manufacturing <strong>and</strong> use, to<br />
the “ultimate” disposal of the product.<br />
For services, CP implies incorporating <strong>environment</strong>al<br />
concerns into designing <strong>and</strong> delivering<br />
services.<br />
savings of Rs. 51.0 million were achieved, in addition<br />
to a 34% reduction in pollution load, 20%<br />
reduction in fuel consumption <strong>and</strong> 12% reduction<br />
in electricity consumption. The most significant<br />
CP measures implemented are:<br />
◆ increasing batch size by 10% to 1100 kg of<br />
naphthalene, producing immediate savings of<br />
about Rs. 11.3 million per year;<br />
◆ installing a pressure-reducing valve to lower<br />
steam pressure from 12 to 5 kg/cm 2 in the reduction<br />
vessel, resulting in savings of about Rs.0.8<br />
million per year;<br />
◆ stopping the mother liquor blower in order to<br />
control the flow of the liquor to the incinerator in<br />
the zero discharge, resulting in savings of about<br />
Rs. 30,600 per year;<br />
◆ increasing the amino concentration to 45°Be by<br />
five-effect steam evaporator, resulting in the<br />
reduction of caustic consumption, of mother<br />
liquor generation, of the sulphuric acid requirement<br />
in isolation <strong>and</strong> of the cost of incineration,<br />
as well as better recovery of Glauber’s salt. This<br />
option has led to savings of about Rs. 3.7 million<br />
per year. Reduction of steam consumption alone<br />
has produced savings of Rs. 1.9 million per year.<br />
ADCI Dyechem Pvt. Ltd., Ahmedabad<br />
(reactive dyes manufacturer)<br />
M/s. ADCI Dyechem Pvt. Ltd. is a dye manufacturer<br />
with a production capacity of about 2400<br />
million MT/year of reactive dyes (40 different<br />
dyes). During the CP project 32 cleaner production<br />
measures were identified, of which 17 were<br />
implemented. The unit invested Rs. 1.0 million<br />
in implementing CP measures <strong>and</strong> achieved<br />
annual net savings of Rs. 2.25 million, in addition<br />
to a 56% reduction in pollution load <strong>and</strong> 65%<br />
reduction in water consumption. The most significant<br />
CP measures implemented are:<br />
◆ using the first wash water from filter press cake<br />
washing for wet cake dissolution;<br />
◆ modifying product cake washing from three<br />
times (1000 litres of water per batch) to a single<br />
1500-litre wash;<br />
◆ using the first wash water from spray dryer<br />
washing for wet scrubbing of the spray drier. After<br />
concentration, the scrubbing liquor is spray dried<br />
to recover the product.<br />
Alps Chemicals Pvt. Ltd., Ahmedabad (acid<br />
dye manufacturer)<br />
M/s. Alps Chemicals Pvt. Ltd. is a small-scale<br />
UNEP Industry <strong>and</strong> Environment April – September 2004 ◆ 45