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industry and environment - DTIE

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Chemicals management<br />

gases such as chlorine, sulphur dioxide <strong>and</strong> trioxide,<br />

nitrogen oxides, <strong>and</strong> fumes of acid <strong>and</strong> organic<br />

solvents. Much of the time, these by-products of<br />

unit processes are recovered subject to the cost of<br />

recovery <strong>and</strong> their market potential. They are normally<br />

gases like SO 2 , HCl (hydrochloric acid, or<br />

hydrogen chloride) <strong>and</strong> organic products. If they<br />

are not recovered, they cause air pollution. A 100%<br />

recovery rate is not possible; the unrecovered product<br />

is vented from the stack.<br />

Particulate matter emissions from the drying<br />

<strong>and</strong> grinding operation are another source of pollution.<br />

Concentrations can be as high as 500-600<br />

mg/litre. Flue gas from the boiler is also a source of<br />

air pollution in this sector. Very high particulate<br />

matter emissions of the dyestuff in powder form<br />

are a major source of air pollution from the<br />

dyestuff production plant.<br />

An emission st<strong>and</strong>ard exists for most types of<br />

gases <strong>and</strong> particulate matter (e.g. 50 mg/litre in<br />

the case of particulate matter).<br />

Management of gaseous emissions<br />

To meet emission limits, gases <strong>and</strong> fumes emitted<br />

from the stack are generally scrubbed using<br />

packed bed type scrubbers. Most SMEs in this<br />

sector are unable to comply with the st<strong>and</strong>ards for<br />

source or fugitive emissions.<br />

Cleaner production in the chemical<br />

<strong>industry</strong> (dye, dye intermediates<br />

<strong>and</strong> pharmaceuticals)<br />

Significant <strong>environment</strong>al degradation has<br />

occurred in various parts of India due to rapid<br />

development/industrialization. Greater <strong>environment</strong>al<br />

awareness <strong>and</strong> activism in all quarters,<br />

accompanied by the economic liberalization promoted<br />

by the Indian government, have left Indian<br />

SMEs struggling for survival. In the past decade<br />

they have experienced a financial crunch at the<br />

same time as growing pressure to improve their<br />

<strong>environment</strong>al performance. End-of-pipe treatment<br />

of waste <strong>and</strong> emissions is being promoted,<br />

but with only limited success since it is cost-intensive.<br />

And changing the form of the waste is not the<br />

same thing as eliminating it. Over the decade only<br />

a few cleaner production initiatives have been<br />

undertaken, mostly as demonstration projects. A<br />

few of these are briefly described below.<br />

A cleaner production demonstration project<br />

was carried out in 12 chemical plants in 2001-02<br />

by the National Productivity Council, located at<br />

Vapi, Gujarat. Participants were from the dye, dye<br />

intermediates <strong>and</strong> pharmaceutical sectors. During<br />

the project 788 cleaner production measures were<br />

identified. By the end of 2002, 380 had been<br />

implemented.<br />

Implementing these measures required an<br />

investment of Rs. 8.5 million. This investment is<br />

expected to yield Rs. 40 million per year through<br />

improved productivity <strong>and</strong> reduced <strong>environment</strong>al<br />

load. The measures implemented include:<br />

◆ use of purer grade naphthalene <strong>and</strong> of iron powder<br />

having higher activity, leading to an annual net<br />

saving of Rs. 0.18 million in addition to a 50%<br />

reduction of organics in sludge;<br />

◆ substitution of inorganic for organic acid in<br />

UNEP’s definition of cleaner production<br />

the final isolation of NMJ (a dye intermediate)<br />

following purification, leading to an annual<br />

net saving of Rs. 4.3 million <strong>and</strong> a 50% reduction<br />

of effluent organic load;<br />

◆ modification of acetonyl sulphonyl chloride<br />

(ASC) cake washing (static material water<br />

seeping through, changed to continuous stirring<br />

of material while washing), leading to a<br />

reduction of water <strong>and</strong> caustic consumption<br />

<strong>and</strong> improved quality of ASC. This measure<br />

produced economic savings of Rs. 6.6 million<br />

per year for an investment of Rs. 10,000;<br />

◆ increasing the height of the distillation column,<br />

leading to improved recovery of isopropyl<br />

alcohol at a bulk drug manufacturing<br />

unit. This measure produced an annual net<br />

saving of Rs. 0.8 million for an investment of<br />

Rs. 0.38 million.<br />

Ishan Dye Chem Ltd. (copper phthalo<br />

cyanine dye intermediate manufacturer)<br />

M/s Ishan Dye Chem Ltd. is a small-scale dye<br />

intermediate unit that manufactures copper<br />

phthalo cyanine (CPC), which is further<br />

processed to produce alpha <strong>and</strong> beta blue dyes.<br />

The unit produces 100 tonnes of CPC per<br />

month. A cleaner production process was introduced<br />

in order to reduce water consumption,<br />

recover solvent effectively <strong>and</strong> conserve energy.<br />

Major CP measures implemented are:<br />

◆ installation of a rotary air lock in a raw material<br />

feeding hopper to reduce solvent losses in<br />

the work atmosphere. This measure resulted in<br />

annual net savings of Rs. 1.8 million for an<br />

investment of Rs. 0.1 million;<br />

◆ increasing vacuum pressure from 400 to 700<br />

mm Hg for improved recovery of trichlorobenzene<br />

(TCB) from the heated mass in the vannulator.<br />

This measure, which required an<br />

investment of Rs. 0.5 million, led to annual net<br />

savings of Rs. 1.3 million.<br />

Metrochem Industries Ltd., Ahmedabad<br />

(H-acid dye intermediate manufacturer)<br />

M/s. Metrochem Industries Ltd. is a dye intermediate<br />

manufacturing <strong>industry</strong> with a production<br />

capacity of about 60 tonnes of H-acid (an important<br />

dye intermediate produced from naphthalene)<br />

per month. During the CP project 27 cleaner<br />

production measures were identified, of which 12<br />

were implemented. The unit invested Rs. 2.8 million<br />

in implementing the CP measures. Annual<br />

Cleaner production is the continuous application<br />

of an integrated preventive <strong>environment</strong>al<br />

strategy to processes, products <strong>and</strong> services to<br />

increase overall efficiency, <strong>and</strong> to reduce risks to<br />

humans <strong>and</strong> the <strong>environment</strong>. Cleaner production<br />

can be applied to the processes used in any<br />

<strong>industry</strong>, to products themselves, <strong>and</strong> to various<br />

services provided to society.<br />

For the production process, CP results from<br />

one or a combination of conserving raw materials,<br />

water <strong>and</strong> energy; eliminating toxic <strong>and</strong> dangerous<br />

raw materials; <strong>and</strong> reducing the quantity<br />

<strong>and</strong> toxicity of all emissions <strong>and</strong> wastes at source<br />

during the production process.<br />

For products, CP aims to reduce the <strong>environment</strong>al,<br />

health <strong>and</strong> safety impacts of products<br />

over their entire life cycles, from raw materials<br />

extraction, through manufacturing <strong>and</strong> use, to<br />

the “ultimate” disposal of the product.<br />

For services, CP implies incorporating <strong>environment</strong>al<br />

concerns into designing <strong>and</strong> delivering<br />

services.<br />

savings of Rs. 51.0 million were achieved, in addition<br />

to a 34% reduction in pollution load, 20%<br />

reduction in fuel consumption <strong>and</strong> 12% reduction<br />

in electricity consumption. The most significant<br />

CP measures implemented are:<br />

◆ increasing batch size by 10% to 1100 kg of<br />

naphthalene, producing immediate savings of<br />

about Rs. 11.3 million per year;<br />

◆ installing a pressure-reducing valve to lower<br />

steam pressure from 12 to 5 kg/cm 2 in the reduction<br />

vessel, resulting in savings of about Rs.0.8<br />

million per year;<br />

◆ stopping the mother liquor blower in order to<br />

control the flow of the liquor to the incinerator in<br />

the zero discharge, resulting in savings of about<br />

Rs. 30,600 per year;<br />

◆ increasing the amino concentration to 45°Be by<br />

five-effect steam evaporator, resulting in the<br />

reduction of caustic consumption, of mother<br />

liquor generation, of the sulphuric acid requirement<br />

in isolation <strong>and</strong> of the cost of incineration,<br />

as well as better recovery of Glauber’s salt. This<br />

option has led to savings of about Rs. 3.7 million<br />

per year. Reduction of steam consumption alone<br />

has produced savings of Rs. 1.9 million per year.<br />

ADCI Dyechem Pvt. Ltd., Ahmedabad<br />

(reactive dyes manufacturer)<br />

M/s. ADCI Dyechem Pvt. Ltd. is a dye manufacturer<br />

with a production capacity of about 2400<br />

million MT/year of reactive dyes (40 different<br />

dyes). During the CP project 32 cleaner production<br />

measures were identified, of which 17 were<br />

implemented. The unit invested Rs. 1.0 million<br />

in implementing CP measures <strong>and</strong> achieved<br />

annual net savings of Rs. 2.25 million, in addition<br />

to a 56% reduction in pollution load <strong>and</strong> 65%<br />

reduction in water consumption. The most significant<br />

CP measures implemented are:<br />

◆ using the first wash water from filter press cake<br />

washing for wet cake dissolution;<br />

◆ modifying product cake washing from three<br />

times (1000 litres of water per batch) to a single<br />

1500-litre wash;<br />

◆ using the first wash water from spray dryer<br />

washing for wet scrubbing of the spray drier. After<br />

concentration, the scrubbing liquor is spray dried<br />

to recover the product.<br />

Alps Chemicals Pvt. Ltd., Ahmedabad (acid<br />

dye manufacturer)<br />

M/s. Alps Chemicals Pvt. Ltd. is a small-scale<br />

UNEP Industry <strong>and</strong> Environment April – September 2004 ◆ 45

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