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Implementation of Metal Casting Best Practices - EERE - U.S. ...

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I. Aluminum <strong>Casting</strong> Facility-1<br />

Plant Pr<strong>of</strong>ile<br />

Aluminum <strong>Casting</strong> Facility-1 produces castings for a variety <strong>of</strong> products including engine<br />

products, exercise equipment, and power tools. It produces 40 million pounds <strong>of</strong> aluminum<br />

castings per year and employs a variety <strong>of</strong> casting processes including die, permanent mold, sand,<br />

lost foam, and pressurized lost foam. Due to the size <strong>of</strong> this facility, the analysis focused on the<br />

pressurized lost foam operation. However, senior management did provide the assessment team<br />

with an example <strong>of</strong> a benefit they experienced by incorporating the results from a <strong>Metal</strong> <strong>Casting</strong><br />

R&D project into its die casting operation.<br />

The 20,000 square feet pressurized lost foam facility is highly automated. The steps in the<br />

operation process are similar to traditional lost foam, although there are a few additional steps.<br />

The process begins with fabricating patterns from polystyrene beads. The patterns are then<br />

coated with a carefully controlled refractory material by dipping them into a slurry. Once the<br />

coating has dried, the patterns are placed into a drum-like flask and packed in molding medium<br />

via a programmed vibratory system which fills the space between the pattern and the flask walls.<br />

A robotic arm then picks up the flask and places it into one <strong>of</strong> the pressure vessels. Once inside<br />

the pressure vessel, another robotic arm pours the aluminum into the vessel, and the polystyrene<br />

pattern begins to vaporize. The molten metal is delivered to the lost foam pressure line using a<br />

launder system and is held in a natural gas-fired reverberatory furnace. Once pouring is complete,<br />

the lid <strong>of</strong> the vessel is closed and 150 psi <strong>of</strong> pressure is applied for 15 minutes as the casting<br />

solidifies. A robotic arm removes the solidified casting from the vessel and quenches it in water.<br />

The casting then automatically moves to the cleaning and finishing room. 60<br />

Aluminum <strong>Casting</strong> Facility-1 has a staff dedicated to identifying opportunities for energy savings,<br />

and implementing projects to achieve these energy savings. The annual energy bill for the entire<br />

plant is approximately $10 million per year mostly attributable to the need to melt, hold, and<br />

distribute molten metal. 61 The plant has an active program in place to identify compressed air<br />

leaks and identify any other wasteful practices, and has installed high-efficiency lighting and<br />

motors. The furnaces and the launder system were properly insulated and covered.<br />

Onsite Assessment<br />

The format <strong>of</strong> the site visit followed the same as the others. The facility was aware <strong>of</strong> the<br />

services <strong>of</strong>fered by IAC that are part <strong>of</strong> the ITP <strong>Best</strong><strong>Practices</strong> subprogram. However, due to its<br />

large size, it does not qualify for IAC’s services. As the assessment team found at other plants,<br />

the management at Aluminum <strong>Casting</strong> Facility-1 was unaware <strong>of</strong> the free suite <strong>of</strong> <strong>Best</strong><strong>Practices</strong><br />

s<strong>of</strong>tware tools. They also were unaware <strong>of</strong> the Save Energy Now efforts. Learning about their<br />

benefits, Aluminum <strong>Casting</strong> Facility-1 decided to apply for an Energy Savings Assessment<br />

(ESA) <strong>of</strong> both its die casting and lost foam facilities. They were awarded however at the time <strong>of</strong><br />

drafting this report the assessment results were not yet available.<br />

75

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