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Implementation of Metal Casting Best Practices - EERE - U.S. ...

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During their site visit, the team from Case Western took metal samples and measurements from<br />

various points in the melting operation to check metal quality. They determined that the die<br />

casting dip wells had four times the amount <strong>of</strong> oxides than that was present at the induction<br />

furnace. The large amount <strong>of</strong> oxides in the metal can lead to porosity formation in the casting,<br />

which is a significant cause <strong>of</strong> scrap. To increase total productivity, these oxides need to be<br />

eliminated prior to the metal entering the die cavity.<br />

Initially the facility’s management thought that Case Western’s findings were a mistake or a<br />

misreading. The facility enlisted a second opinion from GKS Engineering. However, the results<br />

from GKS were identical to Case Western’s research findings. GKS recommended that<br />

Aluminum <strong>Casting</strong> Facility-1 install a degassing head, which they did. Once the degassing head<br />

was installed, the oxides were virtually eliminated. Participation in university research has<br />

proven critical to this facility’s success and has yielded a reduction in scrap rate due to oxides<br />

entrapped in their aluminum castings.<br />

Participated in Save Energy Now (SEN) Effort<br />

As part <strong>of</strong> this effort, Aluminum <strong>Casting</strong> Facility-1 was provided background information on the<br />

free tools and services <strong>of</strong>fered by the ITP <strong>Best</strong><strong>Practices</strong> program, including the Save Energy<br />

Now solicitation that encourages large energy-using plants to apply for an Energy Saving<br />

Assessment (ESA). Because <strong>of</strong> this, Aluminum <strong>Casting</strong> Facility-1 decided to apply and was<br />

selected to be a recipient <strong>of</strong> ESA. A team <strong>of</strong> ESA experts visited their plant for several days and<br />

audited their energy use. The ESA experts were all <strong>Best</strong><strong>Practices</strong>-qualified specialists who are<br />

skilled at using the <strong>Best</strong><strong>Practices</strong> assessment and analysis s<strong>of</strong>tware tools (PHAST, AirMaster+,<br />

MotorMaster, etc.). The purpose <strong>of</strong> their assessment at Aluminum <strong>Casting</strong> Facility-1 was to<br />

identify immediate opportunities to save energy and money, primarily by focusing on the process<br />

heating systems (melting, holding, molten metal handling) and steam use (for fabricating the<br />

EPS patterns). These processes were responsible for over half <strong>of</strong> the plant’s energy use. The<br />

facility realized that savings achieved in these systems could dramatically reduce their annual<br />

$10 million energy bill. Aluminum <strong>Casting</strong> Facility-1 realized that fine-tuning these systems<br />

may cost little but <strong>of</strong>fers the potential to yield large savings. Facility management also believed<br />

that quick successes with optimizing these systems could lead to significant long-term savings<br />

for their facility. The results <strong>of</strong> this assessment were not available at the time <strong>of</strong> writing this<br />

report. To learn more about ESA results, please visit the Save Energy Now results site at:<br />

http://www.eere.energy.gov/industry/saveenergynow/partners/results.cfm.<br />

2. Conclusion<br />

The assessment team found the operating practices at Aluminum <strong>Casting</strong> Facility-1 to be among<br />

the best in all the plants evaluated. The facility and its management have participated and<br />

benefited from the research from the CMC and ITP <strong>Metal</strong> <strong>Casting</strong> portfolio. These efforts have<br />

proven valuable to the facility’s success in lost foam and die casting. The efforts at UAB for<br />

measuring pattern permeability and pattern coatings have significantly benefited facility’s<br />

pressurized lost foam production plant. Through their cost share efforts working with UAB and<br />

Flow Science, this facility was able to work out the bugs with the Flow 3D model and make it<br />

more useful for correcting design flaws before they cause manufacturing and quality problems.<br />

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