Implementation of Metal Casting Best Practices - EERE - U.S. ...
Implementation of Metal Casting Best Practices - EERE - U.S. ...
Implementation of Metal Casting Best Practices - EERE - U.S. ...
Create successful ePaper yourself
Turn your PDF publications into a flip-book with our unique Google optimized e-Paper software.
During their site visit, the team from Case Western took metal samples and measurements from<br />
various points in the melting operation to check metal quality. They determined that the die<br />
casting dip wells had four times the amount <strong>of</strong> oxides than that was present at the induction<br />
furnace. The large amount <strong>of</strong> oxides in the metal can lead to porosity formation in the casting,<br />
which is a significant cause <strong>of</strong> scrap. To increase total productivity, these oxides need to be<br />
eliminated prior to the metal entering the die cavity.<br />
Initially the facility’s management thought that Case Western’s findings were a mistake or a<br />
misreading. The facility enlisted a second opinion from GKS Engineering. However, the results<br />
from GKS were identical to Case Western’s research findings. GKS recommended that<br />
Aluminum <strong>Casting</strong> Facility-1 install a degassing head, which they did. Once the degassing head<br />
was installed, the oxides were virtually eliminated. Participation in university research has<br />
proven critical to this facility’s success and has yielded a reduction in scrap rate due to oxides<br />
entrapped in their aluminum castings.<br />
Participated in Save Energy Now (SEN) Effort<br />
As part <strong>of</strong> this effort, Aluminum <strong>Casting</strong> Facility-1 was provided background information on the<br />
free tools and services <strong>of</strong>fered by the ITP <strong>Best</strong><strong>Practices</strong> program, including the Save Energy<br />
Now solicitation that encourages large energy-using plants to apply for an Energy Saving<br />
Assessment (ESA). Because <strong>of</strong> this, Aluminum <strong>Casting</strong> Facility-1 decided to apply and was<br />
selected to be a recipient <strong>of</strong> ESA. A team <strong>of</strong> ESA experts visited their plant for several days and<br />
audited their energy use. The ESA experts were all <strong>Best</strong><strong>Practices</strong>-qualified specialists who are<br />
skilled at using the <strong>Best</strong><strong>Practices</strong> assessment and analysis s<strong>of</strong>tware tools (PHAST, AirMaster+,<br />
MotorMaster, etc.). The purpose <strong>of</strong> their assessment at Aluminum <strong>Casting</strong> Facility-1 was to<br />
identify immediate opportunities to save energy and money, primarily by focusing on the process<br />
heating systems (melting, holding, molten metal handling) and steam use (for fabricating the<br />
EPS patterns). These processes were responsible for over half <strong>of</strong> the plant’s energy use. The<br />
facility realized that savings achieved in these systems could dramatically reduce their annual<br />
$10 million energy bill. Aluminum <strong>Casting</strong> Facility-1 realized that fine-tuning these systems<br />
may cost little but <strong>of</strong>fers the potential to yield large savings. Facility management also believed<br />
that quick successes with optimizing these systems could lead to significant long-term savings<br />
for their facility. The results <strong>of</strong> this assessment were not available at the time <strong>of</strong> writing this<br />
report. To learn more about ESA results, please visit the Save Energy Now results site at:<br />
http://www.eere.energy.gov/industry/saveenergynow/partners/results.cfm.<br />
2. Conclusion<br />
The assessment team found the operating practices at Aluminum <strong>Casting</strong> Facility-1 to be among<br />
the best in all the plants evaluated. The facility and its management have participated and<br />
benefited from the research from the CMC and ITP <strong>Metal</strong> <strong>Casting</strong> portfolio. These efforts have<br />
proven valuable to the facility’s success in lost foam and die casting. The efforts at UAB for<br />
measuring pattern permeability and pattern coatings have significantly benefited facility’s<br />
pressurized lost foam production plant. Through their cost share efforts working with UAB and<br />
Flow Science, this facility was able to work out the bugs with the Flow 3D model and make it<br />
more useful for correcting design flaws before they cause manufacturing and quality problems.<br />
80