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Vaporization of JP-8 Jet Fuel in a Simulated Aircraft Fuel Tank ...

Vaporization of JP-8 Jet Fuel in a Simulated Aircraft Fuel Tank ...

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In the beg<strong>in</strong>n<strong>in</strong>g <strong>of</strong> the test, the liquid fuel was heated to 30°F above its <strong>in</strong>itial<br />

temperature and allowed to vaporize until quasi-equilibrium is achieved. From figure<br />

6.4, it can be seen that the amount <strong>of</strong> fuel evaporated was similar to the amount <strong>of</strong> fuel<br />

stored <strong>in</strong> the ullage, because at this po<strong>in</strong>t there was little condensation. Once dew po<strong>in</strong>t<br />

conditions were reached, the condensation rate <strong>in</strong>creased and the mass <strong>of</strong> fuel stored <strong>in</strong><br />

the ullage leveled <strong>of</strong>f even though the mass <strong>of</strong> fuel evaporated still <strong>in</strong>creased, as it did for<br />

the duration <strong>of</strong> the test. As the climb to altitude was <strong>in</strong>itiated, the mass <strong>of</strong> fuel stored <strong>in</strong><br />

the ullage began to decrease rapidly as ullage gas was vented due to the pressure<br />

differential between the ullage and the atmosphere. The ambient air temperature was<br />

decreas<strong>in</strong>g quite rapidly at this po<strong>in</strong>t due to the <strong>in</strong>creas<strong>in</strong>g altitude, and the fuel tank<br />

temperatures began to decrease, caus<strong>in</strong>g an <strong>in</strong>crease <strong>in</strong> the rate <strong>of</strong> condensation and a<br />

decrease <strong>in</strong> the mass <strong>of</strong> fuel stored <strong>in</strong> the ullage. Upon descend<strong>in</strong>g from cruise, air<br />

entered through the vents due to the pressure differential and diluted the ullage vapor<br />

mixture. When the fuel tank was back to sea level atmospheric pressure, the fuel tank<br />

temperatures were about 15°F cooler than at the beg<strong>in</strong>n<strong>in</strong>g <strong>of</strong> the test, and the mass <strong>of</strong><br />

fuel stored <strong>in</strong> the ullage was about 0.002 kg less than at the beg<strong>in</strong>n<strong>in</strong>g.<br />

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