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In-flight upset - 154 km west of Learmonth, WA, 7 October 2008,

In-flight upset - 154 km west of Learmonth, WA, 7 October 2008,

In-flight upset - 154 km west of Learmonth, WA, 7 October 2008,

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Figure 2: Aircraft track and key eventsAfter returning the aircraft to FL370, the <strong>flight</strong> crew commenced actions to dealwith multiple ECAM caution messages. These were:• NAV IR 1 FAULT: the required action presented on the ECAM was to switchthe ATT HDG (attitude heading) switch from the NORM position to the CAPTON 3 position. The crew completed the required action and cleared the message.• F/CTL PRIM 3 FAULT 13 : the required action was to select the <strong>flight</strong> controlprimary computer 3 (FCPC 3) OFF and then select it back ON. The crewcompleted the required action and cleared the message.• NAV IR 1 FAULT: this message had reappeared at the top <strong>of</strong> the ECAM withno additional required actions, and was cancelled by the crew.• F/CTL PRIM 1 PITCH FAULT: there was no required action associated withthis message. The crew confirmed that there was no associated fault light on theoverhead panel and then started reviewing the <strong>flight</strong> control page on theECAM’s system display.1.1.4 Second in-<strong>flight</strong> <strong>upset</strong> (0445:08)At 0445:08 (1245:08 local time), while the crew were responding to the ECAMmessages, the aircraft commenced a second pitch-down movement, reaching amaximum pitch angle <strong>of</strong> about 3.5° nose down. The <strong>flight</strong> crew described the eventas being similar in nature to the first event but less severe. The captain promptlyapplied back pressure on his sidestick to arrest the pitch-down movement. He saidthat, consistent with the first event, this action initially had no effect, but soon afterthe aircraft responded normally. FDR data showed that the <strong>flight</strong> control system didnot respond to <strong>flight</strong> crew inputs for at least 2 seconds, and that the aircraftdescended 400 ft over 15 seconds before returning to FL370.13F/CTL is used for fault messages associated with the <strong>flight</strong> control system. PRIM is the term usedin fault messages and operational procedures to refer to a <strong>flight</strong> control primary computer (FCPC).- 4 -

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