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Assessment of the Bill Emerson Memorial Bridge - FTP Directory ...

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42. Song, W., Giraldo, D.F., Clayton, E.H., Dyke, S.J. and Ciacedo, J.M. (2006).Application <strong>of</strong> ARMAV for modal identification <strong>of</strong> <strong>the</strong> <strong>Emerson</strong> <strong>Bridge</strong>.Proceedings <strong>of</strong> <strong>the</strong> Third International Conference on <strong>Bridge</strong> Maintenance, Safetyand Management (IABMAS06), Porto, Portugal.43. Vold, H., Kundrat, J., Rocklin, G.T. and Russel, R. (1982). A multi-input modalestimation algorithm for mini-computers, SAE Technical Paper Series, N.820194.44. Wang W., Chen G. and Hartnagel B. (2007). A. real-time condition assessment <strong>of</strong><strong>the</strong> <strong>Bill</strong> <strong>Emerson</strong> cable-stayed bridge using artificial neural networks. Proceedings<strong>of</strong> SPIE, April, Volume 6529.45. Wilson E.L., Yuan, M.W., and Dickens, J.M. (1982). Dynamic analysis by directsuperposition <strong>of</strong> Ritz vectors. Earthquake Engineering and Structural Dynamics.1982, 10, pp.813-823.46. Wilson J.C. and Liu T. (1991). Ambient vibration measurements on a cablestayedbridge. Earthquake Engineering and Structural Dynamics, 20, pp. 723-47.47. Wilson J.C. and Gravelle W. (1991). Modeling <strong>of</strong> a cable-stayed bridge fordynamic analysis. Earthquake Engineering and Structural Dynamics. 20, pp. 707-721.48. Xu Y., Ko J.M. and Zhang W. (1997). Vibration studies <strong>of</strong> Tsing Ma suspensionbridge. ASCE Journal <strong>of</strong> <strong>Bridge</strong> Engineering, 2, pp.149-56.99

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