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XV-15 litho - NASA's History Office

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as could be accepted for tests in the 40- by 80-foot wind test section.<br />

The wind tunnel test of the <strong>XV</strong>-<strong>15</strong> was made a required part of the TRRA project in<br />

the first Project Plan that was issued in 1972. This requirement was carried forth in<br />

later revisions of the Plan and through execution. The technical rationale for this test<br />

was strong. It provided an opportunity to evaluate the loads, performance, and aerodynamic<br />

characteristics, as well as the function of the mechanical, electrical, and<br />

hydraulic systems under operational conditions in the controlled environment of the<br />

wind tunnel and without risk to a flight crew. Yet there were arguments against the<br />

wind tunnel test. These detractors questioned the wisdom of exposing the aircraft to<br />

the risks associated with a tied-down wind-on experiment. 27 They were also concerned<br />

about the impact of the additional costs to conduct the test as well as delaying<br />

flight activity. There were even discussions questioning whether the real motivation<br />

was to show that the 40- by 80-foot wind tunnel was still a viable tool for developing<br />

new types of aircraft. In any event, the wind tunnel test was a critical milestone that<br />

needed to be reached before embarking on the flight evaluation program.<br />

The ability to operate the <strong>XV</strong>-<strong>15</strong> N702NA as an unmanned wind tunnel model<br />

was provided as the aircraft was designed and constructed. Mounting locations<br />

for the wind tunnel struts (called “hard points”) were built into the aircraft’s<br />

structure at the lower surface of each wing and the tail. Provisions were made for<br />

the installation of remote operation devices for the engines and flight controls.<br />

The external supply source connections were installed for hydraulic and electrical<br />

power used to operate the control systems during wind tunnel testing with the<br />

engines not operating. For tests with the engines running, the aircraft’s enginedriven<br />

electrical and hydraulic systems were used.<br />

Prior to entering the tunnel, the aircraft’s fuel tanks were drained and filled with<br />

nitrogen (to reduce the risk of an explosion), and the fuel lines capped (the wind<br />

tunnel “external” fuel supply was connected directly to the engines, bypassing<br />

the fuel tanks). Actuators for the remote operation were installed. The landing<br />

gear was retracted and the gear doors were closed during the test.<br />

Figure 45 shows the <strong>XV</strong>-<strong>15</strong> mounted on the three-strut support system in the<br />

Ames 40- by 80-foot wind tunnel. To assure safe operation, crew training was<br />

conducted during the ground tiedown tests at the contractor’s facility with the<br />

remote control systems installed. At Ames, the TRRA simulation math model<br />

was modified to represent operation in the wind tunnel and remote operations<br />

were simulated to evaluate emergency operating procedures. The only failure<br />

identified that could cause a dangerous condition was a simultaneous dual engine<br />

failure in high-speed helicopter mode flight (with the nacelles above 85 degrees).<br />

The emergency procedure required to avoid potentially destructive loads called<br />

27 An aircraft constrained by a wind tunnel mounting system might be subjected to operating conditions<br />

not normally encountered nor sustained in flight. These unusual conditions could produce<br />

airloads, moments, and torques that exceed allowable design limits and result in structural failure.<br />

57

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