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Refinery - II M&I SD Oct-Nov 2018

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Chennai Petroleum Corporation Limited (A group company of Indian Oil)<br />

Technical - Inspection<br />

Chennai Petroleum Corporation Limited (A group company of Indian Oil)<br />

Technical - Inspection<br />

16-F-03- CO Boiler:<br />

Complete replacement of pre-fabricated & pre-dried out convection module in 3 segment along with tubes &<br />

header boxes.<br />

Combustion chamber partial casing plate replacement & complete relining of combustion dual refractory (5”<br />

hot face + 5” back up) with new anchors.<br />

Both burner housing replacement (One new assembly & other one fabricated)<br />

RLA study of the CO boiler/connected piping & IBR license renewal<br />

Internal painting in 16-C-16 / 51/ 52/ 53 were renewed with tank liner painting as per CPCL painting system<br />

XI.<br />

WFMPT was carried out for 08 nos. columns/ vessels viz. 16-C-59, 16-C-60, 16-C-259, 16-C-260, 16-C-271,<br />

16-C-272, 16-C-273 & 16-C-275,<br />

Optimix feed nozzle 8” ring CS material mix-up segments were replaced with A335 P5 pipe.<br />

Reactor top outlet24” pipe line has wall thickness of 9.52 mm(Sch.:20) in vertical portion and 17.48<br />

mm(Sch.:40)in horizontal portion.<br />

Reactor top 24”outlet pipe line to 16-C-01 inlet U/S 1.5” TG point CS material was replaced with A335 P11.<br />

HCO draw pipe line from 16-C-01 to 16-C-03 10”/6” and reflux 8” pipe line were replaced and hydrotested at<br />

9.6KSC and 10.5KSC respectively.<br />

Pipe support location in plant inside pipe rack were checked and corroded & pitted area in pipe lines were<br />

replaced. Mild pitted area at support locations were provided with RF Pad.<br />

Cooling water supply and return 24” pipe line at U/G to A/G interface portion below technological structure<br />

replaced due to leak.<br />

77 nos. Safety Valves were pre-pop tested, dismantled, serviced, reconditioned and bench tested.<br />

16-F-03: Combustion Chamber Refractory<br />

16-X-01- CO Stack:<br />

Refractory re-lining of 0-10.0 m & 50-60.0 m elevation.<br />

Stack health assessment by engaging M/s Varishitha Concrete Ltd.<br />

Complete stack external painting.<br />

3.1.3 Equipment & Piping<br />

16-F-03: Convection Module Prefab & Erection<br />

External patch for about 9.0 m 2 was provided on 16C01 shell (EL+<br />

16-C-01: Patch Work<br />

26400 mm to 29400 mm) due to bulging. All 5 nos. structured<br />

packing beds were replaced. CRO spray nozzles of distributor above<br />

Bed 5 ( EL+16435) was also replaced as per PE recommendations.<br />

16-C-61: CBD vessel was replaced.<br />

16-C-12: CO Boiler IBD- Internal Patch welding was carried out due to<br />

severe erosion corrosion.<br />

16-C-59: Debutaniser- External patch welding was done at four<br />

locations due to severe CUI at insulation support ring & stiffener<br />

rings.<br />

16-C-274: Sand Filter Coalescer- Sacnd carryover with LPG was observed during start-up and observed with<br />

poor fixing of sand retainer mesh. New mesh was properly fixed and boxed up.<br />

Complete insulation removal of the columns (16C02, 16C03, 16C58 & 16C59) was carried out followed by<br />

painting and insulation renewal.<br />

External patch for about 12.0 m 2 was provided on 16-C-59 (at 4 elevations near insulation support ring).<br />

3.1.4 Exchanger<br />

One exchanger & 15 nos. of coolers were taken for maintenance as pre-shutdown activity.<br />

Two fin fan coolers (16-E-108A1/D2) were anticipated for replacement & four fin fan coolers were anticipated<br />

for retubing. However procurement of 6 nos. of fin fan coolers 16-E-108A1/A2/C1/C2/D1/D2 had been done<br />

based on maintenance decision in order to save the time in case of retubing.<br />

RLA study of the exchangers (16-E-04A/B, 16-E-07) were carried out & offered for IBR authorities for extension<br />

of license.<br />

NFT inspection was deployed for assessing the tube condition in the following Exchangers:-<br />

Number of Exchangers retubed in this Shutdown:-<br />

<br />

02nos. - 16-E-05 A & 16-E-05 B<br />

Number of coolers / condensers tube bundles retubed in this Shutdown:-<br />

<br />

S NO. EXCHANGER NO. EXCHANGER NAME<br />

1 16-E-108 B1 Main Column OVHD Fin Cooler<br />

28 nos. - 16-E-52, 16-E-52A, 16-E-53, 16-E-054, 16-E-56C, 16-E-57, 16-E-63A, 16-E-63B, 16-E-109A,<br />

16-E-109B, 16-E-109C, 16-E-109D, 16-E-109E, 16-E-109F, 16-E-110A, 16-E-110B, 16-E-121A, 16-E-<br />

121B, 16-E-159A, 16-E-159B, 16-E-251A, 16-E-251B, 16-E-253, 16-E-254, 16-E-259, 16-E-263A, 16-E-<br />

263B, 16-E-264<br />

Number of Exchanger/ Coolers tube bundles replaced in this Shutdown:-<br />

Coolers<br />

Air Fin Coolers<br />

108D2<br />

: 03 nos – 16-E-56 A, 16-E-56 B & 16-E-64<br />

: 06nos. - 16-E- 108A1, 16-E- 108A2, 16-E-108 C1, 16-E-108-C2, 16-E- 108D1, 16-E-<br />

FLUIDIZED CATALYTIC<br />

CRACKING UNIT (FCCU – PLANT 16)<br />

346<br />

<strong>Refinery</strong> - <strong>II</strong> M&I S/D <strong>Oct</strong>-<strong>Nov</strong> <strong>2018</strong> - Inspection Report<br />

<strong>Refinery</strong> - <strong>II</strong> M&I S/D <strong>Oct</strong>-<strong>Nov</strong> <strong>2018</strong> - Inspection Report<br />

347

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