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Refinery - II M&I SD Oct-Nov 2018

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Chennai Petroleum Corporation Limited (A group company of Indian Oil)<br />

Technical - Inspection<br />

15-F-02 A: SCHEMATIC SKETCH OF REPLACEMENT PORTIONS<br />

2.2.4 15-F-02B VACUUM HEATER<br />

Coil Arrangement:<br />

Chennai Petroleum Corporation Limited (A group company of Indian Oil)<br />

Technical - Inspection<br />

Description Number of tubes Tube size Tube MOC<br />

4.5” OD X 6.01 mm Thk. -26 nos.<br />

2 Passes X 28 tubes/ each pass<br />

Radiant HC Coil<br />

6.625” OD X 7.11 mm Thk.-1 no. A 335 Gr.P9<br />

Total-56 tubes<br />

8.625” OD X 8.18 mm Thk.-1 no.<br />

40 studded tubes +<br />

Convection HC coil<br />

4.5” OD X 6.01 mm Thk.- 48 tubes A 335 Gr.P9<br />

8 plain tubes<br />

Brief History:<br />

In 2007 decoking short shutdown, the carburized/holed out arch roof casing plate at west manway location was<br />

replaced & ceramic fibre lining was renewed at that location. Due to severe bowing/oxidation scales & high<br />

surface hardness, 3 nos. of radiant coils were replaced.<br />

Emergency shutdown was made on August 2011 due to convection tube leak due to carburization on account of<br />

inner side coke deposit. In total, 26 nos. out of 42 nos. of convection tubes were replaced. Utilizing this<br />

opportunity 2 nos. of radiant tubes were also replaced due to bulges & low thickness. Complete arch roof plate<br />

was replaced & ceramic module was relined.<br />

In 2012 M&I shutdown, Bottom, middle & top bank intermediate tube sheets were replaced as recommended<br />

earlier due to multiple cracks along with end tube sheets. Stack tip retainer ring alone was replaced. Addition of<br />

top two rows convection studded tubes; all burner replacement with low NOx type & burner floor plate along with<br />

refractory replacement jobs were taken up as a part of rev<strong>amp</strong> project activities. 10 nos. of radiant tubes were<br />

removed and 6 nos. new tubes (with increased size) were added.<br />

CRUDE DISTILLATION UNIT<br />

(CDU/ VDU-<strong>II</strong> PLANT-15, 17, 18)<br />

- Convection section return bends<br />

Convection section<br />

replacement.<br />

return<br />

bends replacement.<br />

(South side)<br />

(South side)<br />

Ref-<strong>II</strong> vacuum section was taken on emergency shutdown in <strong>Nov</strong>’ 2016 due to convection shock tube leak in 15-<br />

F-02B. Failure was attributed due to internal coke formation & localized overheating due to absence of velocity<br />

steam provision at the shock tubes. Bottom bank all 8 nos. of tubes were replaced & recommended to<br />

reintroducing velocity steam connection. External carburization/dis-coloration was noticed on 5 - 6 nos. of<br />

radiant tubes (earlier dis-coloration was noticed on-stream) & same was recommended to monitor. Radiant<br />

internal brick lining was renewed for the top 3 rows only & external patches were provided on shell external<br />

surface. Partial arch roof replacement with module was carried out.<br />

Upon completion of decoking radiant bottom, arch roof, convection and stack manways were opened & inspected.<br />

Following major jobs were carried out.<br />

9 nos. of Radiant tube replacement.<br />

Replacement of 8 nos. of convection shock tubes & 4 nos. return bends due to low thickness.<br />

Radiant Shell casing (EL + 7424 m to EL +12148 m) replacement along with refractory renewal.<br />

98<br />

<strong>Refinery</strong> - <strong>II</strong> M&I S/D <strong>Oct</strong>-<strong>Nov</strong> <strong>2018</strong> - Inspection Report<br />

<strong>Refinery</strong> - <strong>II</strong> M&I S/D <strong>Oct</strong>-<strong>Nov</strong> <strong>2018</strong> - Inspection Report<br />

99

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