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Refinery - II M&I SD Oct-Nov 2018

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`<br />

Chennai Petroleum Corporation Limited (A group company of Indian Oil)<br />

Technical - Inspection<br />

Chennai Petroleum Corporation Limited (A group company of Indian Oil)<br />

Technical - Inspection<br />

Soot blower target plate found dislodged & fallen in the gap<br />

between lining & studded tube.<br />

<br />

Radiant end tubesheet refractory was left as such. However damaged refractory at bottom section of ETS was<br />

relined on all both sides.<br />

<br />

Radiant return bend header box refractory lining was found in good condition.<br />

Jobs Carried Out:<br />

Radiant Section:<br />

<br />

<br />

<br />

<br />

<br />

Without disturbing the radiant tubes, complete internal<br />

refractory removal was carried out. 30% of west side casing<br />

plate was also cut & removed during the decoking process.<br />

Complete side wall casing plate & end plates were removed<br />

completely.<br />

Dislodged Target Plate & Refracory damages<br />

Floor plate with refractory was retained since condition of refractory found satisfactory.<br />

The prefabricated casing plates along with internal anchors & shelf plate setup was installed in 24 segments.<br />

Subsequent to casing plate replacement, radiant section refractory relining was carried out under M/s. Phisem<br />

consultant supervision as per Phisem drg. No: P430-1012 Rev.1.<br />

<br />

<br />

<br />

Radiant tube creep measurement found to be satisfactory within 2% of OD enlargement. UT Gauging of<br />

radiant coil was carried out and noticed with min. of 5.3 (B5)/ 6.7 (A14)/ 7.7 (B15)/ 9.0 (B16) mm thickness<br />

(Size: 4”/6”/8”/10”) against 6.0/7.1/8.2/9.7 mm original thickness and found satisfactory.<br />

In situ metallography (IMG) test was carried out on all 4 pass outlet tubes 10” tube number A16, B16,C16,D16<br />

and found satisfactory.<br />

Radiant tube hanger support conditions during initial inspection is given below.<br />

Tube No.<br />

1st support<br />

from north<br />

15-F-02A Tube support Condition<br />

2nd support<br />

from north<br />

3rd support<br />

from north<br />

D13,14 Bolt & cl<strong>amp</strong> missing Bent Bolt missing<br />

D 11,12 Intact Normal Intact<br />

C 7,8 Tube hanger missing Bolt missing Tube hanger missing<br />

C 1,2 Tube in bend condition Bolt missing Normal<br />

A 1,2 Normal Normal Not rested<br />

A 5,6 Not rested Normal Normal<br />

CRUDE DISTILLATION UNIT<br />

(CDU/ VDU-<strong>II</strong> PLANT-15, 17, 18)<br />

B 1,2 Bend condition Normal Bolt missing<br />

15-F-02 A: View of Casing plate prefabrication, Painting & refractory jobs after erection<br />

B 3<br />

Normal<br />

Support rested on bottom tube<br />

support<br />

B 5,6 Not rested Normal<br />

Normal<br />

Support rested on bottom tube<br />

support<br />

<br />

Hip section casing was patch repair done at few locations. Also ISMC200 was partially replaced for about 1m<br />

length.<br />

A 14,15 Normal Holding vertical cl<strong>amp</strong> missing Normal<br />

** Missing hanger supports were removed by contractor for enable the casing replacement.<br />

<br />

Hip section castable refractory was completely renewed by shuttering after exposing all v anchors. Few<br />

carburized anchors were replaced with new ones. The HIP section hanger support location was wrapped with<br />

ceramic fibre blanket before lining the castable refractory.<br />

<br />

All 12 nos. skin point thermocouples were renewed (B16, A16, B10, A10, D16, C16, C10 & D10 and shock<br />

tubes - two nos) & provided at new locations. Skin point thermocouples were checked by Maint. – Instruments<br />

and found satisfactory. Thermocouple welds were DP Tested and Ceramic blanket was wrapped at the<br />

thermocouple coil before box-up.<br />

<br />

The skin thermocouples were not provided as per the requirement. The radius of cover plate was not welded<br />

properly as there was gap between tube and gap.<br />

<br />

Damaged Burner no. 1, 4, 5, 8 & 12 muffle blocks were replaced. Refractory relining around the burner muffle<br />

blocks were carried out.<br />

<br />

Damaged burner tips were replaced with OEM tips.<br />

<br />

Additional holes were provided on the HIP section casing plate for easy draining of water at external support<br />

beam in order to drain the accumulated water.<br />

15-F-02 A: Casing Replacement & Refractory renewal jobs<br />

92<br />

<strong>Refinery</strong> - <strong>II</strong> M&I S/D <strong>Oct</strong>-<strong>Nov</strong> <strong>2018</strong> - Inspection Report<br />

<strong>Refinery</strong> - <strong>II</strong> M&I S/D <strong>Oct</strong>-<strong>Nov</strong> <strong>2018</strong> - Inspection Report<br />

93

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