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WATER JET CONFERENCE - Waterjet Technology Association

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equired, and although it is convenient in other water jetting situations, in a fixed<br />

installation this is not always found to be desirable.<br />

5. The speed of the pump could be increased or decreased with a variable speed motor,<br />

thus increasing or decreasing the volume of water. Eventually, the last solution was<br />

used, but as only two pressures were required, then a double wound stator was used<br />

and it was found that without changing the nozzles, simply by changing a connection<br />

on the motor winding, that the motor would rotate at either 1450 rev/min or 960<br />

rev/min. The pressure being approximately inversely proportional to the flow,<br />

therefore, the higher speed rotation of the pump gave 10,005 PSI and lower rotational<br />

speed of the pump gave a pressure of 6,525 PSI. This simplified the operation of the<br />

speed changes or pressure changes for the operator. He could merely move a lever on<br />

the starter which was indicated 'high pressure' or 'low pressure'.<br />

So, as a door was removed, it was examined and the pump started at the required<br />

speed. Eventually, after the ovens had been used for about 3 times and all doors were<br />

kept clean by the lower pressure of 6,525 PSI, this saved pump power, use of water,<br />

pump wear, gland wear, nozzle wear and was generally thought to be the most efficient<br />

way of using the jet cleaning system.<br />

DESIGN SOLUTIONS<br />

The first cleaning machines were to be used on the coke side which generally has<br />

a more difficult problem with door sealing, as the hot coke is passed through this side of<br />

the oven. The coke guide machine is fairly small as it merely has the door extracting<br />

facility; a separate trolley car is towed behind the door extractor, which is quite a simple<br />

openwork structure. There was difficulty to find space to accommodate quite a large<br />

pump, 125 hp unit and a 400 gallon tank. The size of the tank was determined by the<br />

number of cleaning operations or pushing cycles required per shift and in order not to<br />

interrupt the flow of coke pushing, it was planned that the tank would be filled at the<br />

beginning of each shift. The tank was placed as high as possible in the coke guide<br />

machine to give a positive head to the triplex plunger pump, low level alarm and<br />

shutdown facility ensured that low level of the tank would either stop or inhibit the<br />

starting of the pump, this protected the pump from dry running.<br />

High pressure water is fed through a pulsation damper and a high pressure hose to<br />

the nozzle cleaning lance. Special attention had to be paid to the gland of the pump to<br />

ensure that the coal dust and ash dust which penetrates every corner of the door<br />

extracting machines did not affect the plunger seals and crankcase oil seals (see figure 6.)<br />

The tracing motion which originally carried the scrapers had to be redesigned to<br />

take the water jetting lance. The first design of the tracing motion carried two cleaning<br />

lances each on cleaning one half of the track around the periphery of the door seal.<br />

Eventually, this was replaced by one single lance, which rotated completely around the<br />

periphery of the door seal.<br />

OPERATING EXPERIENCES & CHANGES TO DATE<br />

Early use of the door cleaner in production had some problems with the lance<br />

becoming bent due to the buildup of tar on the door plug. This led to refinements on the<br />

hydraulic drive of the tracing motion. A relief valve was fitted so that if an obstruction<br />

161

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