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WATER JET CONFERENCE - Waterjet Technology Association

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Bottom notch diameter was determined both indirectly by measuring the volume<br />

of cuttings removed during notching and directly by means of a down hole caliper. The<br />

volume of cuttings were measured by recording the change in height of settled material in<br />

a 55 gallon drum used as a settling tank. The down hole caliper measured the insertion<br />

distance of a spring steel tongue, Figure 5, which was forced into a horizontal orientation<br />

over a series of rollers when engaged. The caliper was manually operated from the<br />

surface by pushing a sliding rod downward relative to a fixed position caliper body which<br />

could be lowered to the desired depth in the injection hole.<br />

Initial analysis indicated horizontal separation should initiate from 2 foot diameter<br />

bottom notches at an injection hole pressure of approximately 20 psi. Initial attempts at<br />

injection required pressures in excess of 40 psi to induce slurry flow indicating that<br />

renotching of each injection hole followed by immediate slurry injection was required.<br />

The resistance to separation propagation at the tip of the notch was attributed to excessive<br />

filter cake build-up resulting from slurry leak off occurring over a period of a few weeks.<br />

By inducing propagation immediately after notching this build up would be avoided.<br />

Higher injection pressures also lead to leakage up along the casings. Leakage into<br />

the overburden in general often reached the surface in the vicinity of injection holes. In<br />

the course of modifying the notching system to achieve the desired performance over 20<br />

leaks to the surface were encountered requiring the development of a routine leak seal off<br />

procedure. Initially portland cement grout was pumped under low pressure into the<br />

leaking injection hole, allowed to set and through drilled in preparation for another<br />

notching attempt at slightly greater depth. This operation proved time consuming and<br />

made subsequent notching operation more difficult.<br />

A second method of sealing off leaks was therefore adopted and refined. A thick<br />

slurry containing swelling particles of varying diameter was pumped into the leaking<br />

injection hole and injection pressure was gradually increased allowing these particles to<br />

bridge in the leak channel and seal off with filter cake build-up. Upon attaining a<br />

satisfactory pressure (35 to 40 psi) the hole was renotched followed by immediate<br />

separation propagation.<br />

Deformation analysis of an infinite half space indicated injection pressure<br />

should be inversely proportional to notch diameter. The notching mechanism was<br />

therefore modified to increase notch diameter to 4 feet. The jet system was now designed<br />

to erode with a jet of 2 percent bentonite slurry in an air medium (figure 6). Slurry was<br />

pumped down a 2 inch diameter line to a 1/2 inch diameter horizontal jet (figure 7).<br />

Slurry and cuttings and excess air then returned up a 1 1/2 inch diameter return line from<br />

a sump beneath the jet to a settling tank on surface. The air medium was maintained by a<br />

slow inflow of compressed air at the casing collar. Back pressure was maintained by a<br />

flow control valve throttling the return flow at the settling tank. Excess air bubbled into<br />

the return line in the sump and was released at the settling tank. This system was used to<br />

notch and propagate separations from intermediate injection holes. The initial 4 foot<br />

notches were each expanded until they intersected the perimeter of the block. Each<br />

separation was therefore propagated until it obtained a diameter of approximately 26 ft.<br />

320

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