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ANP PROJECT QUARTERLY PROGRESS REPORT<br />

and frozen seal ran for 550 hr before<br />

it had to be stopped because of a valve<br />

failure in <strong>the</strong> loop. Average operating<br />

conditions during t,his run were:<br />

Pump suction pressure 5 to 15 psig<br />

Pump discharge pressure 35 to 50 psig<br />

Shaft speed 1500 rpm<br />

Flow 15 gpm<br />

Packing temperature 750 to 1050OF<br />

Temperature at extreme<br />

end of frozen seal 600 to 800°F<br />

The packing of <strong>the</strong> pump was made up<br />

of Inconel braid with mixtures of<br />

graphite powder and nickel powder<br />

bet,ween <strong>the</strong> layers of braid. The pump<br />

shaft was coated with Stellite No. 6.<br />

Operation of <strong>the</strong> pump was charac-<br />

terized by frequent power surges of<br />

<strong>the</strong> driving motor because of shaft<br />

seizing in <strong>the</strong> seal area. Tricresyl<br />

phosphate and lead glass were periodi-<br />

cally injected into <strong>the</strong> seal as<br />

lubricants, with indeterminant results.<br />

Postrun examination of <strong>the</strong> shaft<br />

showed very severe scoring in <strong>the</strong><br />

frozen seal region (0.056 in. on <strong>the</strong><br />

diameter of <strong>the</strong> 1 1/2-in. shaft).<br />

The second run of this pump was of<br />

600 -hr duration. Loop shutdown was<br />

caused by leakage of <strong>the</strong> pump flange.<br />

Changes made in <strong>the</strong> pump and in <strong>the</strong><br />

operating procedure before this run<br />

were:<br />

1. pump shaft resurfaced to remove<br />

scoring of first run,<br />

2. packing changed to nickel-foil<br />

wrapped braid with graphite powder<br />

be tween packing 1 ayer s,<br />

3. no lubricants injected.<br />

Operation was much smoo<strong>the</strong>r than<br />

that of <strong>the</strong> first run. This seemed<br />

to be primarily <strong>the</strong> result of closer<br />

temperature regulation of <strong>the</strong> frozen-<br />

seal area. It was found that 750 to<br />

800°F was <strong>the</strong> most satisfactory range<br />

for relatively smooth operation.<br />

Leakage of solid fluoride from <strong>the</strong><br />

sen1 at <strong>the</strong>se temperatures varied<br />

approximately from 1 t o 3 g/day. The<br />

packing temperature was maintained at<br />

1050°F.<br />

18<br />

A stop-start technique for <strong>the</strong><br />

frozen seal was developed during this<br />

second run. Upon turning off <strong>the</strong><br />

iiiotor power, <strong>the</strong> pump coasts freely to<br />

a stop. However, <strong>the</strong> shaft becomes<br />

immovable in approximately 30 seconds.<br />

Therefore calrod heating is applied to<br />

<strong>the</strong> frozen seal area and <strong>the</strong> tempera-<br />

ature brought to an indicated 850°F.<br />

Theseal <strong>the</strong>n loosens, and <strong>the</strong> operation<br />

may be resumed with no leakage. Timing<br />

is important, since <strong>the</strong> application<br />

of too much heat may result in heavy<br />

seal leakage. A quick mean5 of<br />

cooling <strong>the</strong> seal, such as an air<br />

blast, must be used if <strong>the</strong> frozen<br />

seal is completely removed.<br />

A second Durco pump has been<br />

modified to include a combination<br />

packed and frozen seal. This pump has<br />

accumulated 84 hr of operation at<br />

1200°F and flow rates up to 60 gpm.<br />

Operation of this pump has been<br />

very difficult because of unexplained<br />

seizing in <strong>the</strong> seal area. Temperature<br />

rise5 along <strong>the</strong> seal area indicate<br />

that <strong>the</strong> seizing is taking place in<br />

<strong>the</strong> packing area of <strong>the</strong> seal. This<br />

cannot be definitely concluded,<br />

however, since <strong>the</strong> shaft has not been<br />

examined in that area.<br />

Some stop-start data were obtained<br />

during one of <strong>the</strong> runs. It appeared<br />

that a very definite temperature range<br />

(750 to 820°F in this case) was needed<br />

for remote loosening of <strong>the</strong> shaft and<br />

subsequent startup without leakage.<br />

The start-stop procedure was repeated<br />

five times, and successful operation<br />

followed each trial. However, this<br />

performance could not he duplicated<br />

in later trials. Part of this incon-<br />

sistency is thought to be caused by<br />

<strong>the</strong> chip retainer, which is being<br />

removed for <strong>the</strong> next run.<br />

One o<strong>the</strong>r change-is being made in<br />

<strong>the</strong> seal geometry in an attempt to<br />

obtain more consistent operation.<br />

The radial clearance between shaft<br />

and wall in <strong>the</strong> frozen seal region is<br />

being increased from 0.010 to 0.040<br />

in. to more closely duplicate <strong>the</strong>

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