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design of <strong>the</strong> first combination seal<br />

purrlp, discussed above, which ran<br />

sa t,i s fa c to ri 1 y .<br />

Pump with Frozen-Sodium Seal.<br />

Approximately 4000 hr of operation<br />

had been accumulated when <strong>the</strong> test<br />

of <strong>the</strong> pump with <strong>the</strong> frozen-sodium<br />

seal had to be terminated because of<br />

leaking flanges and failure of a<br />

<strong>the</strong>rmocouple well. The final run<br />

was of LOOO-hr duration at a pump<br />

temperature of 1P00'F.<br />

Postrun examination of <strong>the</strong> pump<br />

showed no measurable wear of <strong>the</strong><br />

shaft in <strong>the</strong> frozen-seal area. Scoring<br />

of <strong>the</strong> rear face of <strong>the</strong> impeller,<br />

which indicated interference with <strong>the</strong><br />

housing, was very severe and was<br />

probably <strong>the</strong> source of pump noises<br />

during <strong>the</strong> last run.<br />

Allis-Chalmers Pump. During this<br />

quarter <strong>the</strong> Allis-Chalmers pump that<br />

has a hydrostatic bearing was tested<br />

with NaK as <strong>the</strong> system fluid. When<br />

this pump was first tested, <strong>the</strong> shaft<br />

gas seal provided by Allis-Chalmers<br />

was used. The seal consisted of three<br />

Graphitar rings, each of which had<br />

three 120-deg segments. The room-<br />

temperature di ametral clearance between<br />

shaft seal rings was designed to be<br />

between 0.0065 and 0.008 inch. A t<br />

operating conditions (approximately<br />

170 gpm, 45-ft head, and elevated<br />

temperature), <strong>the</strong> diametral clearance<br />

and <strong>the</strong> gas leakage to atmosphere past<br />

<strong>the</strong>se rings were to approach zero.<br />

In <strong>the</strong> first test, <strong>the</strong> gas leakage<br />

past <strong>the</strong> seal was excessive, and a<br />

large amount of gas was entrained in<br />

<strong>the</strong> system fluid. Therefore two<br />

modifications were made to <strong>the</strong> pump:<br />

a rotary face seal was added to<br />

decrease gas leakage to a tmosphere,<br />

and additional baffling, suggested by<br />

Allis-Chalmcrs, was placed in <strong>the</strong><br />

region above <strong>the</strong> pump impeller to<br />

reduce gas entrainmentin system fluid.<br />

The second test revealed that <strong>the</strong><br />

additional baffling did materially<br />

reduced gas en trainmen t in <strong>the</strong> sys tern<br />

fluid and also that <strong>the</strong> rotary face<br />

PERIOD ENDING DECEMBER 10, I952<br />

seal reduced gas leakage toa tolerable<br />

level. The unlubricated rotary face<br />

seal, however, squealed and chattered<br />

aftera very short period of operation.<br />

Fur<strong>the</strong>r testing indicated that <strong>the</strong><br />

seal operating temperature was sensitive<br />

to changes in pump suction pressure,<br />

a condition that may be overcome by<br />

using a balanced bellows seal. These<br />

tests indicate that this pump w i l l<br />

give satisfactory performance when a<br />

good gas seal is incorporated in <strong>the</strong><br />

design. A frozen-sodium gas seal is<br />

presently being fabricated for test<br />

in this pump.<br />

' Laboratory-Size Pump with Gas Seal.<br />

The laboratory-size centrifugal pump<br />

with a gas seal, described previ-<br />

ously,(') has been operated for a<br />

total of 1275 hr with <strong>the</strong> fluoride<br />

fuel NaF-ZrF,-UF, (46-50-4 mole %) at<br />

temperatures up to 1500°F. The average<br />

fluid temperature during this period<br />

was approximately 1350°F. The satis-<br />

factory performance data obtained are<br />

presented in Fig. 2.1. The pump<br />

discharge pressure and pressure drop<br />

across <strong>the</strong> venturi were measured by<br />

means of <strong>the</strong> null-balance level-<br />

indicator system.<br />

The initial difficulty of liquid-<br />

level detection in <strong>the</strong> pump bowl at<br />

high shaft speeds has been overcome.<br />

The turbulence in <strong>the</strong> liquid surface<br />

has been reduced by additional baffling,<br />

and <strong>the</strong> action of <strong>the</strong> probes used<br />

for level detection has been quite<br />

satisfactory up to shaft speeds of<br />

4400 rpm.<br />

The rotary gas seal - Graphitar<br />

No. 30 lubricated with spindle oil<br />

running against hardened tool s tee1 -<br />

has functioned with extremely small<br />

gas leakage and without maintenance<br />

or appreciable wear during <strong>the</strong> total<br />

running time. Oil leakage past <strong>the</strong><br />

seal assembly was collected, and it<br />

was found to amount to less than<br />

1 cm3 per 24-hr period. The only<br />

(l)W. G. Cobb. P. W. Taylor, and G. D. Whitman,<br />

ANP Quar. Prog. Rep. Sept. IO, 1952. ORNL-1375,<br />

p. 16.<br />

19

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