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Evaluation and Repair of Wrought Iron and - Purdue e-Pubs ...

Evaluation and Repair of Wrought Iron and - Purdue e-Pubs ...

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56completed, but before the surface was ground flush to make the welds blend into theoriginal eyebar connection.Eyebar B was modeled to be a worst case scenario <strong>of</strong> section loss due to corrosionin an eyebar end connection. In this eyebar, half the thickness <strong>of</strong> the original eyebar’smaterial was removed from the center two <strong>and</strong> a half inches around the hole <strong>and</strong>perpendicular to the direction <strong>of</strong> loading. Figure 3.28 shows Eyebar B after this materialwas removed <strong>and</strong> prepared for welding.Once this material was removed, the area simulating corrosion needed to be filledwith weld material. To do this an E7024 SMAW 1/8” diameter welding rod was utilizedwith a DC reverse polarity electric source, similar to Eyebar A. An initial pass aroundthe hole in the eyebar <strong>and</strong> along the open edges were placed to create a dam for the fillermaterial, as can been seen in Figure 3.29.Once the initial passes were placed, filler passes were then placed in the open areain the direction <strong>of</strong> loading <strong>of</strong> the eyebar to reduce heat distortion. In between passes thetemperature <strong>of</strong> the base metal was also monitored to ensure the metal was not to hot toweld <strong>and</strong> to reduce the amount <strong>of</strong> heat distortion in the metal. It was necessary to takebreaks <strong>and</strong> allow the metal cool between sets <strong>of</strong> passes. The welds were also cleanedusing a chisel hammer <strong>and</strong> wire brush in between each pass. Figures 3.30 <strong>and</strong> 3.31 showthe eyebar end connection after all the welding was completed.As can been seen in Figure 3.31 there was a slight amount <strong>of</strong> heat distortion <strong>and</strong>curvature in the wrought iron eyebar connection from the filler weld. To straighten thispiece, the eyebar was heated until it was red hot, as seen in Figure 3.32, <strong>and</strong> thenstraightened by striking the eyebar with large hammer. The color <strong>of</strong> the eyebar wassimilar to the color <strong>of</strong> the iron that was heat straightened in the tension testing coupons<strong>and</strong> therefore at the adequate temperature to straighten the iron without inducing

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