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Khawaja Zaheer Ahmed - PDMA

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gates as per WAPDA’s O and M safety Manual. The management<br />

had diverted 150,000-200,000 cusecs to its power-house and<br />

Chashma-Jhelum Link canal and some through its CRBC besides<br />

impounding 0.31 MAF against barrage’s gross capacity of 0.32<br />

MAF.<br />

u) The next major controlled structure downstream was Taunsa<br />

Barrage with an upgraded design discharge capacity of 1.1 million<br />

cusecs; on 2 nd August that barrage passed a seasonal peak<br />

discharge of 959,891 cusecs, but a 2.4 km length of the LMB, next<br />

to Tibba Tie minor, refurbished during 2008-09, collapsed before<br />

the water reached its crest.<br />

v) That breach in turn triggered almost 10 breaches on nearby<br />

Sunawan Bund and 13 breaches on other secondary bunds (5,000<br />

ft) on the banks of T.P. Link Canal and Muzaffargarh Canal during<br />

2-4 th August.<br />

w) The above breaches had diverted 125, 000 cusecs to inundate vast<br />

areas in Muzaffargarh’s Kot Addu sub-division that remained<br />

exposed to an unprecedented havoc for 17 days. The breach was<br />

closed by constructing a new bund within 20 days by 24/7<br />

deployment of machinery and personnel.<br />

x) On the right side, the rising water threatened the various spurs<br />

including spur no 5 upstream Taunsa, initially erected in 1958 at the<br />

time of constructing the barrage with a view to divert the natural<br />

river course.<br />

y) While locals were strongly of the view that right bank escape could<br />

have prevented the LMB disaster, that recourse could not have<br />

given much relief due to modest capacity of 5-10,000 cusecs<br />

especially as peak discharge of 1.1 million cusecs had not reached<br />

Taunsa.<br />

Page 96 of 211

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