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Final Report - VHB.com

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Stills Drive, and Bath Road at the US Route 1 ramps and Gurnet Road all operate at a<br />

LOS D. The other signalized Study Area intersections operate at LOS C or better.<br />

Table 2.2-2. Signalized Intersection Capacity Analysis Summary<br />

(Results reflect overall intersection operations)<br />

2009 Existing DHV<br />

Location v/c* Delay+ LOS^<br />

State Route 196 & I-295 Northbound Ramps 0.48 16 B<br />

State Route 196 & Topsham Fair Mall Road 0.56 25 C<br />

State Route 196 & Mallet Drive 0.51 7 A<br />

State Route 196 & Hamilton Court 0.50 11 B<br />

State Route 196 & US Route 201 0.82 52 D<br />

State Route 196 & Village Drive/Community Way 1.02 30 C<br />

State Route 196 & State Route 24 Connection 0.66 19 B<br />

US Route 201 & Elm Street 0.89 22 C<br />

Maine Street & Pleasant Street 0.58 16 B<br />

Pleasant Street & Church Street 0.96 35 D<br />

Pleasant Street & River Road/Webster Street 0.85 24 C<br />

Pleasant Street & Mill Street/Stanwood Street 1.07 > 100 F<br />

Bath Road & Federal Street/Sills Drive 0.87 46 D<br />

Bath Road & Merrymeeting Plaza 0.52 10 B<br />

Bath Road & Fitch Avenue 0.49 12 B<br />

Bath Road & US Route 1 Ramps/Gurnet Road 0.65 49 D<br />

*Volume-to-capacity ratio<br />

+Delay expressed in seconds per vehicle<br />

^Level of service<br />

Results of the 2009 DHV existing-conditions analyses at the unsignalized<br />

intersections (Table 2.2-3) reveal that many side-street movements along the primary<br />

Feasibility Study corridors operate at poor levels of service (i.e., LOSs E and F). Most<br />

notably, vehicles exiting from side streets onto US Route 201 and Maine Street<br />

experience excessive delays during peak-hour conditions.<br />

Existing Conditions 32

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