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Content2011 - PETRONAS Gas Berhad

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mainly attributable to the enhanced 4 th Term<br />

GPTA resulting in increase of revenue from<br />

propane and butane volumes. Throughput<br />

services revenue also increased by 10.1% to<br />

RM2,724.0 million while revenue from the<br />

utilities business also increased by 7.3% to<br />

RM801.0 million.<br />

Despite the increase in revenue by 9.4%,<br />

the Group continued to operate diligently<br />

by constantly attempting to bring down its<br />

cost of revenue through continuous rigorous<br />

cost optimisation initiatives at all levels of<br />

the organisation. In pursuit of improving<br />

the bottom line, cost saving initiatives on<br />

manpower, materials sourcing, travelling<br />

and purchased services have been carried<br />

out diligently throughout the year by the<br />

management and staff. The practice of being<br />

prudent and doing ‘more with less’ has<br />

become a corporate culture in PGB, befi tting<br />

its status as a public-listed operating unit of<br />

the <strong>PETRONAS</strong> Group.<br />

Financial year 2010/2011 saw the Group’s<br />

overall profi t before tax increased by<br />

52.8% from RM1,243.8 million last year to<br />

RM1,900.3 million, whilst profi t after tax also<br />

increased by 53.0% from RM940.7 million last<br />

year to RM1,439.1 million. Earnings per share<br />

attributable to shareholders of the Company<br />

were at a record high of 72.7 sen from 47.6<br />

sen in the previous year.<br />

GAS PROCESSING & GAS<br />

TRANSPORTATION BUSINESS<br />

Naturally and Faithfully Reliable<br />

The Company’s <strong>Gas</strong> Processing Plants (GPPs)<br />

operated by the Plant Operations Division<br />

(POD) in Kertih and Paka endured a number of<br />

operational challenges coupled with upstream<br />

constraints which resulted in reduced feedgas<br />

supply. During the year under review, an<br />

average of 2,080 million standard cubic feet<br />

per day (mmscfd) of feedgas was processed.<br />

This represents a 3.3% decline compared<br />

to 2,151 mmscfd which was processed in<br />

the last fi nancial year. Our Peninsular <strong>Gas</strong><br />

53 annUaL report 2011<br />

CEO’s Business Review<br />

The Group’s overall profi t before tax<br />

increased by 52.8% from RM1,243.8 million<br />

last year to RM1,900.3 million,<br />

whilst profi t after tax also increased<br />

by 53.0% from RM940.7 million<br />

last year to RM1,439.1 million.<br />

Utilisation (PGU) pipeline network operated<br />

by the Transmission Operations Division (TOD)<br />

also received 336 mmscfd of gas from the<br />

Malaysia-Thailand Joint Development Area,<br />

lower by 2.0% compared to previous year.<br />

As a result, sales gas delivered to customers<br />

at 2,146 mmscfd was lower than the previous<br />

fi nancial year of 2,178 mmscfd.<br />

The Company managed to maintain reliability<br />

in its plant operations at world class standards.<br />

GPPs’ sales gas reliability was 99.6%. For<br />

ethane, plant reliability was 98.8%, while<br />

plant reliability for propane and butane was at<br />

98.7%, collectively at world class level.<br />

The Company’s product delivery reliability via<br />

its GPPs also recorded convincing numbers<br />

with propane and butane registering 100%<br />

respectively for the year in review. Both<br />

propane and butane recorded 98.7% product<br />

delivery reliability in the previous fi nancial year.<br />

At the same time, the Company’s PGU pipeline<br />

network continued to maintain its excellent<br />

record by achieving 99.97% reliability<br />

exceeding world class standards by all means.

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