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Space Grant Consortium - University of Wisconsin - Green Bay

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entire rocket assembly was too far forward. In order to compensate, weight was placed in<br />

nosecone, around the threaded rod. This stabilized the fully assembled stack, but over-stabilized<br />

the dart. In spite <strong>of</strong> this, the decision was made to fly in this configuration and the launch was a<br />

success. However, the dart noticeably arced into the wind and considerable altitude was lost.<br />

Nevertheless, the basic concept was proven to be viable: the booster-dart junction provided clean<br />

separation and recovery devices deployed properly.<br />

Version II: Drag Coefficient Test Flight Because <strong>of</strong> the overstability <strong>of</strong> “<strong>Green</strong> Bean,” the<br />

drag coefficient <strong>of</strong> the rocket could not be determined from the Midwest Power flight. Version II<br />

was built as a second attempt to gather data. This version focused on the drag coefficient <strong>of</strong> the<br />

booster and dart while they remain in contact.<br />

To get the data, the booster and dart from <strong>Green</strong> Bean were simply screwed together at the joint<br />

between the two. Recovery devices were deployed with motor ejection only, and the flight<br />

computer was used only for gathering data. The flight was technically a success because the<br />

rocket was recovered with no damage. However, a spiraling flight path (caused by the dart’s<br />

inability to rotate) rendered the data useless for the purposes <strong>of</strong> finding the drag coefficient.<br />

Version III: 1.5-inch (38mm) Dart Following the drag coefficient test flight, it was decided that<br />

we should attempt to fly with a smaller diameter dart. Due to the decreased cross sectional area,<br />

a dart <strong>of</strong> this diameter was expected to gain about 1200 feet <strong>of</strong> altitude.<br />

Similar in many respects to the 2.1-inch dart, the 1.5-inch dart included a number <strong>of</strong> changes and<br />

improvements. The stability problem from Version I was corrected by re-evaluating the fin size.<br />

The booster was also rebuilt and reduced in size to minimize its weight. The airframe was also<br />

lengthened in order to provide the necessary volume to store a small parachute and the necessary<br />

fire blanket and shock cord.<br />

The booster was designed so that either dart (2.1-inch or 1.5-inch) could be flown<br />

interchangeably. Changing darts only requires that the transition section be removed and the<br />

alternative size <strong>of</strong> transition be riveted on.<br />

Unfortunately, the test flight <strong>of</strong> this design was not successful. A major malfunction occurred at<br />

approximately 500 feet, immediately following powered flight, and resulted in the loss <strong>of</strong> the<br />

rocket. The cause <strong>of</strong> the failure was insufficient venting <strong>of</strong> the parachute chamber. As the dart<br />

flew higher into the air, the pressure outside the rocket dropped while the pressure inside<br />

remained constant. The pressure difference was sufficient to push the nosecone out <strong>of</strong> the<br />

airframe, deploying the parachute. The parachute deployed while the rocket was moving at<br />

maximum velocity and was immediately torn <strong>of</strong>f. The damage to the dart was irreparable.<br />

However, the booster was recovered in fair condition and both the fin can and transition were reuseable.<br />

Despite this failure, it should be noted that the flight was aerodynamically stable even<br />

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