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F. K. Kong MA, MSc, PhD, CEng, FICE, FIStructE, R. H. Evans CBE, DSc, D ès Sc, DTech, PhD, CEng, FICE, FIMechE, FIStructE (auth.)-Reinforced and Prestressed Concrete-Springer US (1987)

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Table 11.4-4 Moment distribution

Braced frame analysis 417

A B c

l:cols AB BA l:cols BC CB

DF(%) 84 16 15 79 6

FEM(kNm) 0 -651 +651 0 -300 +300

Balance +547 +104 -53 -277 -21

co -26 +52 -10

Balance +22 +4 -8 -41 -3

co -4 +2 -2

Balance +3 +1 -2

l:(kNm) +572 -572 +644 -320 -324 +288

At B: BA: (~col): BC = 15%: 79%: 6%

Fixed end moments (FEM) (Table 11.4-4):

Span AB:

Span BC:

12\~ 82 = 651 kNm

36 ~2 102 = 300 kNm

Since the moments 572 and 644 kNm at the ends of the beam ABare of

comparable magnitude, the sagging moment at the centre of the beam is

very nearly the maximum and has a value of 368 kNm, i.e. (122 x 82/8) -

(572 + 644)/2. This is to be compared with the value of 730 kNm given in

Fig. 4.9-6: Case 3, which assumes zero moment at the support A.

An analysis using the complete storey sub-frame, as in Example

11.4-l(b) with the .full imposed loading on spans AB and CD, gives

values of 573, 642 and 318 kNm for the moments designated AB, BA

and BC respectively. This indicates the relative accuracy of this two-span

sub-frame.

Example 11.4-l(d)

With reference to the braced frame in Example 11.4-1(a) and Fig. 11.4-3,

calculate the maximum sagging moment in the span BC; use the subframe

of Fig. 11.4-1 (f).

SOLUTION

Since the span BC is greater than either of the two adjacent spans, the

solution for BC using the sub-frame in Fig. 11.4-1(f) can also be taken

to give the column design moments (BS 8110: Clause 3.2.1.2.3). This

sub-frame is obviously of much more use when the structure has more

spans than the one being here analysed. Since the analysis of the complete

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