VGB POWERTECH 7 (2020) - International Journal for Generation and Storage of Electricity and Heat
VGB PowerTech - International Journal for Generation and Storage of Electricity and Heat. Issue 7 (2020). Technical Journal of the VGB PowerTech Association. Energy is us! Maintenance. Thermal waste utilisation
VGB PowerTech - International Journal for Generation and Storage of Electricity and Heat. Issue 7 (2020).
Technical Journal of the VGB PowerTech Association. Energy is us!
Maintenance. Thermal waste utilisation
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A journey through 100 years <strong>VGB</strong> | Hydropower | <strong>VGB</strong> <strong>POWERTECH</strong> · Issue 9 (2007)<br />
Maintaining Know-how<br />
20 Member companies from 9 European countries<br />
15,000 MW Run-<strong>of</strong>-river<br />
30,000 MW <strong>Storage</strong> or pumped storage<br />
Figure 3. The large European hydro power<br />
operators practise a systematic<br />
exchange <strong>of</strong> experience under<br />
the ro<strong>of</strong> <strong>of</strong> <strong>VGB</strong>.<br />
During an extensive planned outage in a<br />
pumped storage power plant after 15 years <strong>of</strong><br />
service, it was also time to overhaul the generator<br />
poles. One <strong>of</strong> the tasks was to renew the<br />
field coil frame which is to ensure the gliding<br />
<strong>of</strong> the coil on the pole core. When tendering<br />
<strong>for</strong> the scope <strong>of</strong> services to be provided, this<br />
item was tendered on a functional basis, relying<br />
on the expertise <strong>of</strong> the companies involved.<br />
This was to pave the way <strong>for</strong> an open innovative<br />
solution <strong>for</strong> the problem incurred.<br />
Some weeks after finishing the planned outage,<br />
the field coil frame moved out axially.<br />
Figure 4 shows the problem area with a<br />
movement <strong>of</strong> approx. 25 mm. The field coil<br />
frame seated on the pole core is shown in<br />
Figure 5.<br />
Due to dynamic stresses, the field coil frame<br />
moved out by up to approx. 38 mm. It was<br />
thus indispensable to dismantle the generating<br />
set again, which resulted in several<br />
weeks <strong>of</strong> unavailability. With the support <strong>of</strong><br />
external experts, the structural design was<br />
completely changed. This example was especially<br />
interesting because another shutdown<br />
due to faulty work in the workshop would<br />
have been unavoidable if it had not been possible<br />
to remedy the defects in the workshop<br />
<strong>of</strong> the external contractor during several onsite<br />
checks.<br />
The second example also relates to a pumped<br />
storage plant. Problems arose in connection<br />
with st<strong>and</strong>ard components, namely fastening<br />
screws that were to be built in during a mechanical<br />
inspection outage. These screws were<br />
to fasten the split rings <strong>and</strong> seal rings <strong>of</strong><br />
the pump turbine. Upon delivery, however,<br />
the screws did not have the usual st<strong>and</strong>ardised<br />
properties nor had their quality been assured.<br />
During final assembly, a great number<br />
<strong>of</strong> brittle fractures occurred at the transition<br />
<strong>of</strong> the screw head to the screw shaft (Figur<br />
e 6 ). These fractures were due to a manufacturing<br />
fault. The screw material, a chromium-nickel<br />
alloy, had reached an inadmissibly<br />
high degree <strong>of</strong> hardness.<br />
Moreover, the hexagon socket <strong>of</strong> various<br />
screws was not located centrally (Figure<br />
7).<br />
If the fault had not occurred so early, dynamic<br />
<strong>and</strong> shock-like operating stresses could<br />
have led to machine damage which would<br />
have caused the generating set to be shut<br />
down <strong>for</strong> at least six months because <strong>of</strong> long<br />
component delivery times in particular. This<br />
would have caused fatal losses in revenue in<br />
view <strong>of</strong> the installed capacity <strong>of</strong> the plant<br />
concerned. As a consequence <strong>of</strong> this experience,<br />
it was determined that components that<br />
are material in terms <strong>of</strong> stress <strong>and</strong> function<br />
must be subjected to adequate additional quality<br />
assurance.<br />
Figure 4. Damage at a field coil frame. Axially moving out<br />
<strong>of</strong> the field coil frame.<br />
Figure 5. Field coil frame seated on the pole core.<br />
Figure 6. Brittle fracture <strong>of</strong> a screw head.<br />
Figure 7. Position <strong>of</strong> the hexagon socket out <strong>of</strong> the centre.<br />
<strong>VGB</strong> PowerTech 9/2007 105<br />
84