UWE Bristol Engineering showcase 2015
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Marco Otero<br />
MEng Motorsport <strong>Engineering</strong><br />
Project Supervisor<br />
Dr Yufeng Yao<br />
Drag reduction system development for heavy goods vehicles<br />
Reference Vehicle<br />
Gap Devices<br />
The device used to improve the gap region was to use a<br />
splitter. The aim of the splitter was to prevent flow<br />
interacting across the entirety of the region, stopping a<br />
large wake occurring in the gap. This would reduce the<br />
wake size, causing two smaller wakes either side of it.<br />
The length of the splitter was changed, as was the side<br />
of the gap it was located.<br />
Drag<br />
Count<br />
Drop<br />
50<br />
45<br />
40<br />
35<br />
30<br />
25<br />
20<br />
15<br />
10<br />
5<br />
0<br />
Comparison between best design iterations<br />
Tail Splitter tapered trailer Gap Splitter Underside<br />
Skirting<br />
Underside<br />
Profiling<br />
The reference vehicle used was based on a Volvo tractor with a<br />
standard trailer. Through the use of CFD the drag coefficient of the<br />
vehicle was found to be 0.8. There were three regions on the reference<br />
vehicle highlighted for improvement; the tractor trailer gap, underside<br />
of the vehicle and at the rear of the trailer. These are highlighted on<br />
side velocity contour by the low speed flow in blue. These regions<br />
produced that largest amounts of wake, with an especially large wake<br />
occurring behind the tail face of the vehicle.<br />
Drag<br />
Count<br />
Drop<br />
Tail Edge Devices<br />
Two devices were used to improve the flow at the<br />
rear of the vehicle; splitters and a tapered device.<br />
These aimed to prevent the large wake occurring<br />
behind the vehicle by reducing the interaction in the<br />
region. The splitters had their location and length<br />
changed, whilst the tapered device changed in<br />
length and tapering angle.<br />
Results<br />
A tail end tapered device produced the best result<br />
with a drag count reduction of 49. this reduced the<br />
drag coefficient of the vehicle from 0.800 down to<br />
0.751. When projecting this device for a year in use,<br />
it was found that 113 litres of fuel could be saved<br />
when applying an average mileage of 80’000.<br />
Devices for the underside of the vehicle were not<br />
very effective despite attempts to optimize,<br />
however, their performance is expected to improve<br />
when under crosswind conditions.<br />
Underside Devices<br />
Side skirtings were the device used to improve the<br />
airflow underneath the vehicle. The aim of the<br />
skirtings were to prevent the low velocity flow under<br />
the vehicle from interacting with the high velocity<br />
free stream flow to the sides of the trailer. The<br />
skirtings varied in length and height in an attempt to<br />
optimize the design.<br />
Pressure<br />
(Pa)<br />
Tail Face Pressure Comparison<br />
150<br />
120<br />
90<br />
60<br />
30<br />
0<br />
-9 -6 -3 0 3 6 9<br />
Distance from Centreline (m)<br />
Reference (Pa)<br />
Tapered (Pa)<br />
Project summary<br />
An investigation has been conducted to design and<br />
develop drag reduction systems for a heavy goods<br />
vehicle with the aim of reducing the fuel consumption<br />
by reducing the drag coefficient.<br />
The designs were attached to a reference vehicle and<br />
analyzed through CFD. It was found that devices<br />
attached to the rear of the vehicle provided the most<br />
improved results.<br />
Project Objectives<br />
1. Investigate and learn from all previous work and<br />
research for drag reduction techniques<br />
2. Examine the results from CFD simulations of a<br />
designated reference vehicle.<br />
3. Design drag reduction systems with an iterative<br />
process with a view of design optimisation<br />
4. Perform computation fluid mechanics simulations<br />
and analysis for drag reduction systems<br />
5. Review drag reduction systems with<br />
recommendations for further investigation<br />
Project Conclusion<br />
The aerodynamic performance of a HGV can be easily<br />
improved with the implementation of drag reduction<br />
systems. Devices placed at the rear face of the vehicle<br />
obtained the best results, with a tapered device<br />
reducing the drag coefficient by 49 drag counts. Gap<br />
devices and underside skirtings were less effective,<br />
however would expect a performance under cross wind<br />
conditions.