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UWE Bristol Engineering showcase 2015

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Marco Otero<br />

MEng Motorsport <strong>Engineering</strong><br />

Project Supervisor<br />

Dr Yufeng Yao<br />

Drag reduction system development for heavy goods vehicles<br />

Reference Vehicle<br />

Gap Devices<br />

The device used to improve the gap region was to use a<br />

splitter. The aim of the splitter was to prevent flow<br />

interacting across the entirety of the region, stopping a<br />

large wake occurring in the gap. This would reduce the<br />

wake size, causing two smaller wakes either side of it.<br />

The length of the splitter was changed, as was the side<br />

of the gap it was located.<br />

Drag<br />

Count<br />

Drop<br />

50<br />

45<br />

40<br />

35<br />

30<br />

25<br />

20<br />

15<br />

10<br />

5<br />

0<br />

Comparison between best design iterations<br />

Tail Splitter tapered trailer Gap Splitter Underside<br />

Skirting<br />

Underside<br />

Profiling<br />

The reference vehicle used was based on a Volvo tractor with a<br />

standard trailer. Through the use of CFD the drag coefficient of the<br />

vehicle was found to be 0.8. There were three regions on the reference<br />

vehicle highlighted for improvement; the tractor trailer gap, underside<br />

of the vehicle and at the rear of the trailer. These are highlighted on<br />

side velocity contour by the low speed flow in blue. These regions<br />

produced that largest amounts of wake, with an especially large wake<br />

occurring behind the tail face of the vehicle.<br />

Drag<br />

Count<br />

Drop<br />

Tail Edge Devices<br />

Two devices were used to improve the flow at the<br />

rear of the vehicle; splitters and a tapered device.<br />

These aimed to prevent the large wake occurring<br />

behind the vehicle by reducing the interaction in the<br />

region. The splitters had their location and length<br />

changed, whilst the tapered device changed in<br />

length and tapering angle.<br />

Results<br />

A tail end tapered device produced the best result<br />

with a drag count reduction of 49. this reduced the<br />

drag coefficient of the vehicle from 0.800 down to<br />

0.751. When projecting this device for a year in use,<br />

it was found that 113 litres of fuel could be saved<br />

when applying an average mileage of 80’000.<br />

Devices for the underside of the vehicle were not<br />

very effective despite attempts to optimize,<br />

however, their performance is expected to improve<br />

when under crosswind conditions.<br />

Underside Devices<br />

Side skirtings were the device used to improve the<br />

airflow underneath the vehicle. The aim of the<br />

skirtings were to prevent the low velocity flow under<br />

the vehicle from interacting with the high velocity<br />

free stream flow to the sides of the trailer. The<br />

skirtings varied in length and height in an attempt to<br />

optimize the design.<br />

Pressure<br />

(Pa)<br />

Tail Face Pressure Comparison<br />

150<br />

120<br />

90<br />

60<br />

30<br />

0<br />

-9 -6 -3 0 3 6 9<br />

Distance from Centreline (m)<br />

Reference (Pa)<br />

Tapered (Pa)<br />

Project summary<br />

An investigation has been conducted to design and<br />

develop drag reduction systems for a heavy goods<br />

vehicle with the aim of reducing the fuel consumption<br />

by reducing the drag coefficient.<br />

The designs were attached to a reference vehicle and<br />

analyzed through CFD. It was found that devices<br />

attached to the rear of the vehicle provided the most<br />

improved results.<br />

Project Objectives<br />

1. Investigate and learn from all previous work and<br />

research for drag reduction techniques<br />

2. Examine the results from CFD simulations of a<br />

designated reference vehicle.<br />

3. Design drag reduction systems with an iterative<br />

process with a view of design optimisation<br />

4. Perform computation fluid mechanics simulations<br />

and analysis for drag reduction systems<br />

5. Review drag reduction systems with<br />

recommendations for further investigation<br />

Project Conclusion<br />

The aerodynamic performance of a HGV can be easily<br />

improved with the implementation of drag reduction<br />

systems. Devices placed at the rear face of the vehicle<br />

obtained the best results, with a tapered device<br />

reducing the drag coefficient by 49 drag counts. Gap<br />

devices and underside skirtings were less effective,<br />

however would expect a performance under cross wind<br />

conditions.

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