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FIFTH CANADIAN CONFERENCE ON NONDESTRUCTIVE ... - IAEA

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- 182 -<br />

tube, say 0.5-1.0 metre, so in practice only a few percent of the total PT<br />

volume was inspected for hydride blisters. In contrast, CIGAR inspects<br />

nominally 100% of the PT in a similar period of time. The eddy current gap<br />

operation will be described elsewhere in this conference/6/.<br />

3.3 Problems with CIGARette<br />

After the expected teething problems, CIGARette worked pretty well. A total of<br />

66 PTs were inspected in Pickering 1 and 2, of which about one third showed<br />

reflectors. A further six PTs were inspected in Pickering unit 3. Some of the<br />

problem areas that had to be resolved are discussed below.<br />

Drive Rods/Connectors<br />

The drive rods were loaded by operators working in plastics on the FM<br />

bridge. First, they had to be clean so no slippage occurred in CIGARette's<br />

friction drive. Second, they had to be connected slowly so that the connecting<br />

pins would engage without damage. The connecting pins between the drive rods<br />

and end/head connectors were occasionally damaged during loading. Since about<br />

100 pins are used in each drive rod/head assembly, a critical shortage of<br />

these components arose. Occasionally an inspection had to be performed with a<br />

probe not functioning.<br />

End Connectors<br />

This was a major problem in the early stages with individual wires in the<br />

catinery cable becoming tangled in the pulleys and being cut. Also, the<br />

oscillating rotational scan pattern of the ultrasonic inspection fatigued the<br />

cables at a sharp bend where they came out of the end connector. These<br />

problems were solved by 1) binding the loose wires with tape, and 2) by using<br />

a strain relief spring on the end of the connector.<br />

Rotational Slippage<br />

After only a few inspections it was recognized that progressive rotational<br />

slippage between the drive rod and friction drive (containing the position<br />

readout) could occur. This had serious implications for the ultrasonic<br />

inspection. Blisters were expected only about the 6 o'clock position and a<br />

rotation scan of only 45° was performed about this position. Unrecognized<br />

slippage of only 30° would put the inspection out of the range of the<br />

potential defects. The problem was solved by putting mercury switches in the<br />

end connectors to trigger at the 6 o'clock position to indicate if slippage<br />

occurred.<br />

Operator Comfort<br />

Since CIGARette inspections centre round the operator, fatigue was a potential<br />

problem. The first inspection was done inside the vault in plastic suits, at<br />

great effort. Later, containment penetrations were made, and cabins<br />

constructed, which greatly improved operator conditions.

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