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GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

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DateSeveritySubtypeTitle Description Root cause Corrective Action1 20-Apr-04 Obs F RAV4 Status RAV4 does not indicate"open".2 20-Apr-04 Obs F SS1 Aliveness TestActivated3 20-Apr-04 Obs T Thruster 2 & 14 showslow pressure4 20-Apr-04 Obs F Vatterfly temp sensornoisy reading5 20-Apr-04 Medium Star sensor lack ofacquisitionSS1 aliveness test activated,but mapped to no-op macro64.Thrusters 2 & 14 – very lowpressures (most are 4-5 mV,2 & 14 at -.1) (Saturated.)Vatterfly temp sensor noisyreadingStar sensor not properlyidentifying reference stars;attitude solution form starsensor processing erraticKnown issue with RAV valves(CARD 255).Result of bright objectdetection and subsequentinternal reset of star sensorelectronics.Thruster biasNoise in ECU seen duringground testing.Vehicle initial conditions(mass imbalance,alignments, star sensorsettings) generated datathat the star sensorprocessing algorithm wasunable process successfully.None; valve confirmedopen once thrusters beganworking.Disable this safemode test.Adjust thruster biases sapart of item 005.NoneSwitch to magnetometerbasedattitudedetermination algorithm,adjust magnitude and errorgate thresholds, tunecontrol gyro biases andcross products of inertia,update star sensoralignment matrices.Reacquisition procedureupdated based on-orbitperformance.6 20-Apr-04 Obs T Orbit modelingmismatch.7 21-Apr-04 Obs T Various star tracks thatare not aligned with rollHard to fit orbit modelingwith TDRS GSFC data.Various star tracks that arenot aligned with roll8 21-Apr-04 Obs F SEU observation Multi-bit and single biterrors seen on <strong>Flight</strong>computers; caused Anomaly#034 C&DH B side switchResidual venting of guardtank after launchATC off-tune after initialorbit insertion.Radiation eventsNone; wait for guard tankto complete venting.Tune ATC system (gyrobiases, thruster biases)Increase frequency of SEUmonitoring of CCCA.<strong>Gravity</strong> <strong>Probe</strong> B — <strong>Post</strong> <strong>Flight</strong> Analysis • Final <strong>Report</strong> March 2007 525

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