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GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

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DateSeverity140 20-Jan-05 Minor Large solar flare Large solar event and loss ofguide starSolar event blinded sciencetelescopeSpace vehicle reconfiguredto science configuration.No long term issuesremain.141 20-Jan-05 Obs F MBE in SRE MBE detected at 159501296 Radiation event SRE rebooted142 26-Jan-05 Obs F Increase in CCCA SBEerror rate for 4 minutesSubtypeTitle Description Root cause Corrective ActionIncrease in CCCA SBE errorrate occurring duringsubsequent scrub cycles143 28-Jan-05 obs F MBE in CCCA MBE in CCCA detected at2005/028-17:30144 15-Feb-05 Obs F TRE thermal disturbanceafter DAS switchDecaying oscillation in A-side detector high signalobserved for 15 consecutiveorbits 2005/43-09:05 to2005/44-09:201 Stuck bit in the A-sideflight computerRadiation eventSwitching of SRE-A DASboards caused thermaltransient in TRE-A, resultingin oscillatory Detector Highsignals.After the B-side switch, theplan is to stay on the B-sideflight computer for the restof the mission.MBE found to be in usedarea of Ping buffer. Clearedby patch procedure.No more SRE-A DAS boardswitches are planned. If aswitch is planned, scheduleall switch templates duringGSI, >15 min before GSV.145 15-Feb-05 Obs T Reduction of excessmass flow when gyro Bturned on146 23-Feb-05 GroundObsExcess mass flow reducedseconds after gyro B turnedonF ITF SRE-A time-out 1Hz and 10Hz timeouts inthe ITF SRE-A147 2-Mar-05 Obs T Poor pointingperformance due to SAA148 2-Mar-05 Major B-Side SafemodeRecoveryPoor pointing performanceduring and after SAApassageB-side Safemode recovery.Scrub rate failedExtra ATC control effortrequired to counteract gyroB torque accounts for excessmass flow decrease.Payload processor controlblock was corrupted.If TRE gain is too high, ATCpointing slopes roll over.Gyro B turned off. A-sideperforms better at roll thanB-side, and A-side gyro tostay on for control.Swap Aft SRE-A with SRE-Band attempt transition.Reduced SAA circle from 43to 35 deg and notch filterto 45 deg circle. Reduced A-side gains to 9.2 simultaneous MBEs. Followed B-side recoveryprocedure. Recoveryactivities for this anomalyrolled over to Anomaly 152(CCCA-B Reboot)<strong>Gravity</strong> <strong>Probe</strong> B — <strong>Post</strong> <strong>Flight</strong> Analysis • Final <strong>Report</strong> March 2007 543

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