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GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

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DateSeveritySubtypeTitle Description Root cause Corrective Action49 17-May-04 MAJOR SM activated - High bodyratesHigh body rates observed(pointing) that activatedsafemode following fluxflush. Significant attitudeexcursions observed over anumber of days, degradingcommunications.Thruster 8 failed during highflow conditions followingflux flush. Failed openthruster caused porous plugto choke prior to thruster 8isolation. Most likely rootcause is foreign objectcontamination of thruster 8.Disable Thruster 8 (via TIV).Rebuild and reload ATCcontroller (FSW) to thrusterselection algorithm tocompensate for loss ofthrusters 6, 8. Update andinstall related VMS macros.50 18-May-04 Obs N Vatterfly valve stateupon SM (Anomaly #49)entry changed to closed,but we believe the valveremained openVatterfly valve state uponSM (Anomaly #49) entrychanged to closed, but webelieve the valve remainedopenFeature of ECU telemetrysampling scheme.Non-issue51 20-May-04 Obs T GSS low voltagecheckout failed tocomplete on Gyros 2 & 3Preliminary analysis oftelemetry indicates GSS lowvoltage checkout failed tocompleteHigh gyro charge from initiallevitation off wall (300 mV)Discharge rotor andcontinue tests.52 20-May-04 Obs T Dewar micro-tempvariation at orbital androll period53 21-May-04 Obs T GSS2 reduced stabilitymargins during uncagedcheckoutDewar micro-temp variationat orbital and roll periodResidual thermal couplingto probe from environmentAdjust tank temperatureand watch.Indications of reducedstability margins of sciencegyro 2 during uncagedcheckoutInsufficient stability marginfor gyro 2 at originalmodulation frequency,possibly due todisconnected ground planeIncrease frequency of drivevoltage from 20 to 30 Hz.54 25-May-04 Minor Unexpected turn off ofgyro1 High VoltageGyro1 de-levitatedunexpectedly during Gyro2suspension operation. Thegyroscope was not spinningat a significant rate at thispoint in the mission.Template error; a templatecloning error left the Gyro 1HV off commands in all fourgyro’s “science mission presuspend”templates. ITF hadinsufficient fidelity to detectthis error when tested.100% review of all GSStemplates (~250 items) forcloning errors or misplacedcommands. Correct anyerrors found, retest.<strong>Gravity</strong> <strong>Probe</strong> B — <strong>Post</strong> <strong>Flight</strong> Analysis • Final <strong>Report</strong> March 2007 531

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