12.07.2015 Views

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

GP-B Post-Flight Analysis—Final Report - Gravity Probe B - Stanford ...

SHOW MORE
SHOW LESS
  • No tags were found...

Create successful ePaper yourself

Turn your PDF publications into a flip-book with our unique Google optimized e-Paper software.

DateSeverity84 13-Jul-04 Obs F Slightly elevated solarradiation85 13-Jul-04 Obs F Gyro 2 possible floatingground plane86 15-Jul-04 Obs O Control Gyro A switchedto “High” mode87 16-Jul-04 Obs F High Gyro4 Spindownduring Gyro2 SpinupSlightly elevated solarradiation. Greater than 10MEV particle count.Gyro 2 possible floatingground planeControl Gyro A to “High”mode when previouslycommanded “Low” modeGyro4 spun down from105.8 to 90.77 Hz duringGyro2 spinup88 23-Jul-04 Obs F ATC Cross Coupling Pitch/yaw appears to havesome cross-coupling89 23-Jul-04 Obs T Spin Axis Alignmentrates less than expected90 23-Jul-04 Obs O Anomalous spin down ofgyro 191 25-Jul-04 Obs O Gyro 1 switched toanalog backup modeSubtypeTitle Description Root cause Corrective ActionObserved rates about 25%of expected ratesGyro 1 spun down duringcavity exploration activitieswhile scouting new locationfor full spinup.Gyro 1 switched to spinupanalog backup mode duringHV qualification of spinupposition.92 26-Jul-04 Obs F Large solar flare Large solar flare, >10 MeVprotons peaked at 2000 PFUat 26Jul04 2200ZSun spot activity.Likely cause: disconnect ofground wire to one half ofground plane.Template coding error; ITFhas insufficient fidelity todetect error.Larger than expected gasleakage from spinupchannel of gyro 2 duringgyro 4 spinup.Cross coupling due toremoval of gyro bias errorswhen transitioning out ofgyro hold.Insignificant centrifugalbulge due to low spin speed.Positioning gyroscope tooclose to housing wall duringcavity exploration.Likely root causes: 1)computer heartbeat glitchdue to high processorloading, 2) radiation event inGSS analog electronics, 3)race-mode condition in GSSarbiter.Solar activity in Sun.Level below danger limitsoutlined in Solar Flarecontingincy procedure.WathcNone at this time; stillunder investigation.Correct error and re-delivertemplate.Tune position of to be spunup subsequently (1, 3) tominimize leakage flow.No action required.Manually tune algorithm toproduce alignment indesired direction.Do not command gyroposition to within 2 um ofthe spindown positionduring spinup operations.Recover gyro to digitalsuspension and watchperformance.Safe vehicle per solar flarecontingency procedure.536 March 2007 Chapter D — Summary Table of <strong>Flight</strong> Anomalies

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!