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CONTRACTOR : WHC<br />

WHC-SD-EN-TI-136, Rev. 0 Page 1 of 2<br />

EV ENT FACT SHEET<br />

1. Title: Leaking UST<br />

2. Reporting Organization: Decomissioning Engineering<br />

3. Division/Department/Project: Environmental/<strong>Hanford</strong> Restorati on Oper.<br />

4. Number: D&D/100-O1-90 5. Rev.: 0<br />

6. Date of Event/Time: 6/21/90, 2:00pm Date Discovered: 6/21/90<br />

7. Event Identification:<br />

A) Location of Event: 100-N Service Station (Tank 100-N-SS-27)<br />

B) Plant/Faci'lity Status: Station was out-of-service for testing<br />

---- --------- t---------------------------------------t----- ---<br />

1. Alarm: Facility Type 5. Radiological - Personnel<br />

(False Fire, CAM, CAS, etc.) Contamination, Internal<br />

Z. Regulatory Requirement Deposition, Over Exposure, etc.<br />

(CERCLA, RCRA, WDOE, DOE-RL, 6. Industrial Safety, Personnel<br />

DOE-HQ, etc.) Injury, First Aid, etc.<br />

3. Operating Requirements (OSR, 7. Process Misrouting<br />

CPS, Tech Spec., Procedure 8. Utility System - Electrical,<br />

Administrative, etc.) Steam, Air, Water<br />

4. Release/Spread'- Radioactive 9. Hoisting/Lifting<br />

Contamination/Hazardous 10. Other<br />

Material<br />

C) Event Type: 2 (4OCFR28O.43 [C])<br />

OSR/TS: Nonconformance f)Violation f<br />

CPS: Infraction [3 Violation [<br />

8. Apparent Cause(s) of Event:<br />

Design [3Administrative Control []<br />

Personnel Error [3Procedure [<br />

Material t)Other: [X] Tank age<br />

9. Descriiotion of Event:<br />

While preparing for routine UST Tightness Testing, the 100-N-SS-27 tank<br />

was determined to have a leak. The leak is in the top 10% of the t 'ank<br />

volume (probably at the fill pipe to tank connection) as evidenced by<br />

satisfactory inventory control data for this tank (less than 1%<br />

discrepancy on the last 6 to 12 months). The total release of unleaded<br />

gasoline is estimated at less t han 5 gallons occurring between 6/20/90<br />

(tank fill for testing) and 6/21/90 (discovery of leak).<br />

10. Consequences of Event:<br />

Small release of unleaded gasoline (less than 5 gallons)<br />

A-7400-329 (3/90) (EF) WEFOO5<br />

Event Fact Sheet<br />

C- 18

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