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r - The Hong Kong Polytechnic University

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and a corresponding shear strain of 6.20×10 -3 . At the onset of panel failure, the applied load gradually declined<br />

and the major cracks opened up slowly. <strong>The</strong> failure of the panel was dictated by an aggregate interlock failure as<br />

there was no indication of concrete crushing or reinforcement rupture.<br />

Figure 3 <strong>The</strong> shear stress - shear strain response of SCHPFRC panel<br />

<strong>The</strong> comparison of crack pattern of SCHPFRC and control panels (Susetyo 2009) at failure is shown in Figure 4.<br />

It is noted that the control panel (f’ c = 66MPa), which was made of conventional concrete, has higher<br />

reinforcement ratios (x-direction: reinforcement area of 2061 mm², ρ x = 3.31%; y-direction: reinforcement area<br />

of 260 mm²,ρ y = 0.42% ) compared to the SCHPFRC panel. It was also observed that the failure of the<br />

SCHPFRC panel was caused by the inability of the concrete to transmit the load across the cracks (coarse<br />

aggregate interlock failure) instead of the yielding or fracture of the transverse reinforcement in the conventional<br />

concrete panel. <strong>The</strong> cracks in SCHPFRC panel were significantly fine and well distributed across the face of the<br />

panel, with crack spacing smaller than those observed in the control panel.<br />

Figure 4 Crack patterns at failure of SCHPFRC (left) and conventional concrete (right) panels<br />

<strong>The</strong> principal tensile stress-strain relationships of SCHPFRC and conventional concrete are conducted based on<br />

Mohr’s circle method and shown in Figure 5. Due to higher compressive strength of conventional concrete, the<br />

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