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2012 Annual Report - Media Prima Berhad

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<strong>Media</strong> <strong>Prima</strong> <strong>Berhad</strong><br />

Commitment<br />

to the Environment<br />

MATERIALS MANAGEMENT<br />

In <strong>2012</strong>, the NSTP introduced an ink optimising programme<br />

to promote the most efficient ink usage. Software was<br />

introduced in the digital pages to convert composite black<br />

pixels made from cyan, magenta, yellow and black to 95%<br />

black. This has resulted in 2.5% savings in pages per kg.<br />

In addition to the overall reduction in colour ink<br />

consumption, the software also improves the quality of<br />

reproduction due to less ink being deposited onto the<br />

paper. This produces a clearer look and an enhanced<br />

“perceived” brightness of printed pictures.<br />

In <strong>2012</strong>, NSTP continued to reduce its waste by changing<br />

Computer to Film (CTF) to Computer to Plate (CTP) and<br />

phased out the usage of films. During 2011, CTF was<br />

phased out at our Shah Alam Plant. In <strong>2012</strong>, we rolled this<br />

initiative out at our plants in Prai, Senai and Ajil. This<br />

process reduces chemical waste as the developments of<br />

films are no longer required. The usage of traditional<br />

photographic films, which was a major cost to us, has been<br />

phased out. The CTP also helps to shorten our process flow,<br />

reduces overall processing time and eliminates traditional<br />

film chemistry which was previously one of the dirtiest<br />

waste generators. It also enhances the effect of ink-saver<br />

software due to greater digital control at the<br />

plate-making stage.<br />

During the year, NSTP engaged a specialist to conduct roller<br />

maintenance at our plants in Prai and Shah Alam. This has<br />

led to lower run-up wastage and a reduction in the overall<br />

consumption of newsprint, inks and other production<br />

materials.<br />

Materials usage at NSTP Printing Plants<br />

Material (MT) 2010 2011 <strong>2012</strong><br />

Newsprint 92,003 85,058 87,335<br />

Ink 1,951 1,736 1,739<br />

Our press system upgrade continues to improve in-house<br />

efficiency by reducing start up copies and printing<br />

registrations. These initiatives are ongoing and have further<br />

reduced newsprint wastage and paper consumption in terms<br />

of pages per kg.<br />

We are revamping our newsprint management strategy to<br />

shorten logistics, eliminate unnecessary handling and reduce<br />

overall inventory levels. In order to achieve this, our aim is<br />

to ensure each plant has its own warehouse of adequate<br />

capacity to accomodate Just-In-Time (JIT) deliveries. The<br />

implementation of the JIT principle has saved time and<br />

waste by reducing the warehouse process from our logistics.<br />

This strategy was introduced at our Balai Berita Prai in <strong>2012</strong>.<br />

We hope to repeat this for Balai Berita Shah Alam in 2013<br />

to benefit from the same JIT principle. This is in collaboration<br />

with Malaysian Newsprint Industries (MNI).<br />

Chemical usage, Pre-Press (litres) at NSTP Printing Plants<br />

Chemicals<br />

(Pre-Press,<br />

Main)<br />

Shah<br />

Alam Prai Senai Ajil Total<br />

2010 11,800 12,670 12,760 10,555 45,735<br />

2011 11,565* 12,480 11,095 8,940 49,360<br />

<strong>2012</strong> 10,720 9,570 9,450 9,135 38,875<br />

* higher consumption due to testing of Anocoil plates<br />

WATER MANAGEMENT<br />

Our printing presses adopt a closed system for the press<br />

in which a spray bar is being used. The spraybar system,<br />

or “pulsed dampening system”, generates a fine mist of<br />

fountain solution (water treated with 2% surfactants) to<br />

provide dampening on the printing plates. Compared to<br />

conventional or older spray bar technologies, the system in<br />

use allows for minimal water consumption due to a higher<br />

ratio of dispersed area against amount of water used. We<br />

have modified the system to deactivate the recirculation of<br />

excess fountain solution. This eliminates contaminants from<br />

returning to the main holding tanks. It also ensures that the<br />

spray bar nozzles operate at maximum efficiency as oil,<br />

grease and ink droplets are eliminated from the whole<br />

system.<br />

80<br />

annual<br />

report<br />

<strong>2012</strong><br />

In <strong>2012</strong>, three workshops were held to promote the sharing<br />

of best practices in the workplace. The practice of sharing<br />

information aims to improve productivity and efficiency<br />

in each plant. Daily production reports are published for<br />

each of the plants along with a company average. This<br />

process introduced an element of competition which led to<br />

further improvements.

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