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Membrane and Desalination Technologies - TCE Moodle Website

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<strong>Membrane</strong> Processes for Reclamation of Municipal Wastewater 441<br />

Table 10.5<br />

Consumption of chemical <strong>and</strong> power <strong>and</strong> cost per cubic meter product for<br />

the pilot trials (13)<br />

Item Consumption Cost (S$)<br />

Chemicals<br />

Flocculants (as Al) 2.77 g 0.0174<br />

NaOCl 0.41 g 0.0027<br />

H 2SO 4 0.56 g 0.0019<br />

Subtotal 0.022<br />

Power 0.194 kW-h 0.0248<br />

Total 0.047<br />

Note: S$ Singapore dollar; 1 US dollar = 1.75 Singapore dollar.<br />

3.3.2. Transmembrane Pressure as a Function of Time<br />

The effect of alum dosing concentration on stabilization of the plant operation was<br />

intensively investigated. Figure 10.4 illustrates the TMP of the UF membranes as a function<br />

of time throughout the study under different concentrations of alum dosage. It should be<br />

pointed out that a TMP b<strong>and</strong> appeared because TMP increased with time within one cycle of<br />

the operation mode (20–30 min). The high level <strong>and</strong> low level corresponded to the TMP at the<br />

time immediately before <strong>and</strong> after a backwash operation, respectively. Figure 10.4a indicated<br />

that TMP was 160–210 mbar when alum concentration was 4.8 mg/L <strong>and</strong> the water recovery<br />

was 87.5% at the beginning, then TMP increased to 200–270 mbar as alum concentration<br />

decreased to 1.3 mg/L. TMP tended to slightly increase with time during these two tests.<br />

However, TMP increased sharply <strong>and</strong> was unstable when alum concentration further<br />

decreased to 0.6 mg/L. Figure 10.4b illustrated that TMP was stable in the range of<br />

200–240 mbar as alum concentration was enhanced to 2.5 mg/L during 29 April–6 May.<br />

High TMP on 7 May appeared because the air lock in the feed line caused the feed pump<br />

shutdown; further, the plant shutdown when water level in the feed tank became gradually<br />

low due to the clogging of the strainer. After that, the water recovery was increased to 90.1%<br />

on 10 May while the alum concentration remained the same. TMP had been stable in the<br />

range of 220–260 mbar since then. The results showed that alum concentration was critical<br />

for maintaining stable TMP <strong>and</strong> achieving a smooth operation of the plant, which could be<br />

explained as follows from two aspects.<br />

On the one h<strong>and</strong>, within a backwash interval, a colloidal fouling of the membrane was<br />

formed. In the dead-end UF process for this particular application, alum was dosed into the<br />

feed line just prior to feed pump, then well mixed with the feed inside the pump. It took a few<br />

seconds for the flocculating feed to reach the membranes. Theoretically, flocs formed should<br />

be much larger than the membrane pores before they reached the membrane surface with an<br />

appropriate dosing concentration of alum. During the filtration operation, the flocs gradually<br />

cumulated on the membrane surface <strong>and</strong> formed a temporary cake layer of suspended solids.<br />

After the backwash, the back washable suspended solids could be easily removed <strong>and</strong> the

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