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Membrane and Desalination Technologies - TCE Moodle Website

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<strong>Membrane</strong> Processes for Reclamation of Municipal Wastewater 463<br />

organics. Sodium hypochlorite <strong>and</strong> antiscalant PermaTreat 191 were dosed to the RO feed<br />

line to prevent biofouling <strong>and</strong> scaling to RO membranes (47). A 5-mm pore-size cartridge<br />

filter was installed prior to RO membranes to protect them from foreign materials. Both the<br />

product water from the RO unit <strong>and</strong> the concentrate stream were sent back to the outfall sump<br />

during the study.<br />

7.2.2. UF <strong>and</strong> RO Units<br />

The UF unit contained four HF66–45-XM50P modules installed in parallel from Koch<br />

<strong>Membrane</strong> Systems, Inc. The membranes were polyacrylonitrile hollow fibers with a molecular<br />

weight cut-off of 50,000 Da. The UF unit was designed to operate at high velocity of feed<br />

water by recirculation pump, periodic reversal of the feed flow direction <strong>and</strong> periodic backwashing<br />

sequences to reduce fouling of UF membranes. A Clean-In-Place (CIP) system was<br />

provided for manual chemical cleaning to UF membranes. Kochkleen ® Liquid Detergent was<br />

used for cleaning at pH 10.0 <strong>and</strong> 2% citric acid was used for cleaning at pH 2.0.<br />

The RO unit was constructed with three pressure vessels in 2:1 configuration. Each<br />

pressure vessel held two LFC1-4040 spiral-wound modules that were made of thin film<br />

polyamide composite membranes. A solenoid valve was installed in parallel with the throttled<br />

SS glove valve on the concentrate line <strong>and</strong> was automatically controlled by PLC to periodically<br />

flush the RO membrane surface under high feed flow <strong>and</strong> low pressure. Pressure, flow,<br />

temperature, pH, <strong>and</strong> conductivity indicators <strong>and</strong> online instruments were installed at the RO<br />

unit. There was also a CIP system attached with the RO unit. Two percent citric acid was used<br />

for cleaning at pH 2.0 over 3 h. Then, 1% EDTA was used at pH 12.0 over 1 h operation<br />

followed by 16 h soaking <strong>and</strong> 0.5 h operation (31).<br />

7.2.3. Trial Runs<br />

Preliminary investigation was conducted to monitor the raw feed quality <strong>and</strong> underst<strong>and</strong><br />

the characteristics of the raw feed from March to August 2003 prior to the plant operation.<br />

Samples were collected on hourly basis with an automatic sampler from the discharge outfall<br />

sump for 24 h. pH, conductivity, turbidity, <strong>and</strong> TOC of hourly samples were measured <strong>and</strong><br />

analyses of daily composite samples were conducted.<br />

The study was conducted from September 2003 to February 2004, over 6 months. The<br />

conductivity probing was conducted after RO membranes were loaded into the pressure<br />

vessels to ensure no leakage between the interconnections of membrane elements. The plant<br />

was disinfected thoroughly.<br />

In order to increase RO operating pressure while the RO feed flow remained the same, the<br />

number of RO elements was cut down from previously running with 6–4. One pressure vessel<br />

in RO train was isolated, <strong>and</strong> the RO unit was operated with four elements in series from<br />

November 2003. The operating pressure of RO unit was increased to 100 psi. The operating<br />

conditions of the pilot plant during the study are summarized in Table 10.19.

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