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OCTOBER 19-20, 2012 - YMCA University of Science & Technology

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Proceedings <strong>of</strong> the National Conference on<br />

Trends and Advances in Mechanical Engineering,<br />

<strong>YMCA</strong> <strong>University</strong> <strong>of</strong> <strong>Science</strong> & <strong>Technology</strong>, Faridabad, Haryana, Oct <strong>19</strong>-<strong>20</strong>, <strong>20</strong>12<br />

(iii) Elimination <strong>of</strong> the NVA Activities by making the necessary changes in work methods<br />

Each <strong>of</strong> the 42 activities identified were critically examined to eliminate or reduce the NVA activity associated<br />

with that parameter. In each case, it was observed that, few small changes in the layout at the individual<br />

workstation lead to drastic reduction in the work content. For example, few changes in activity – Placement <strong>of</strong><br />

Front and Rear locators, operation time can be reduced by placing the front and rear locators nearer to the<br />

bonding bay and fixing it onto the super structure <strong>of</strong> the assembly line.<br />

Similar exercise was done for all the 42 activities associated with Existing Method. After evaluating the actual<br />

process it was identified that 5 activities were found to be taking more time than required, and 11 were identified<br />

as non-value added activities. By modification <strong>of</strong> 5 activities and elimination <strong>of</strong> 11 activities, total operation time<br />

<strong>of</strong> 3 minutes 58 seconds was reduced, thereby reducing the number <strong>of</strong> activities from 42 to 31. Hence the total<br />

operation time for Body Side Panel Bonding Process gets reduced to 5 minutes and 53 seconds from 9 minutes<br />

56 seconds. With the changes made in 5 activities and elimination <strong>of</strong> 11 activities there is a reduction <strong>of</strong> 41% <strong>of</strong><br />

operation time.<br />

6. Results and Analysis<br />

Before the new standards were established, an extensive and thorough analysis and review <strong>of</strong> each activity was<br />

conducted in Stage 15 <strong>of</strong> assembly line. The existing process had 42 activities and the time taken to complete the<br />

process was 9 minutes and 39 seconds. After evaluating the actual process it was identified that 5 activities were<br />

found to be taking more time than required, new time standards were established for these activities which are<br />

given Table 1.<br />

Table 1 Details <strong>of</strong> Operation Time Reduction<br />

Operation Name<br />

Existing<br />

Time in<br />

Seconds<br />

Modified<br />

Time in<br />

Seconds<br />

Reduction<br />

Time in<br />

Seconds<br />

Take the front locator 12.6 7.56 5.04<br />

Take the rear locator 12.6 7.56 5.04<br />

Insert rear bottom locator into the top locator 6.84 4.68 2.16<br />

Dispense adhesive 5.76 3.6 2.16<br />

Sealant Application Process time 126.72 86.4 40.32<br />

Total 164.52 109.8 54.72<br />

Table 2 Details <strong>of</strong> Operation Time Elimination<br />

Eliminated Operation Name<br />

Operation Time<br />

in Seconds<br />

Collect the body side panel 12.96<br />

Place the locators on the LH and RH panel 21.6<br />

Inspect the flushness and gap 6.48<br />

Adjust the fitness <strong>of</strong> the panel 4.32<br />

Disengage the Panel 9.36<br />

Place back the panels onto the storage Rack 17.28<br />

Use cotton cloth 0.72<br />

Using the Scuffing Tool 40.32<br />

Clean the scuffed area 57.6<br />

Get the Masking Tape 4.68<br />

Fix the masking tape onto the chassis 9.72<br />

Total 184.32<br />

815

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