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OCTOBER 19-20, 2012 - YMCA University of Science & Technology

OCTOBER 19-20, 2012 - YMCA University of Science & Technology

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Proceedings <strong>of</strong> the National Conference on<br />

Trends and Advances in Mechanical Engineering,<br />

<strong>YMCA</strong> <strong>University</strong> <strong>of</strong> <strong>Science</strong> & <strong>Technology</strong>, Faridabad, Haryana, Oct <strong>19</strong>-<strong>20</strong>, <strong>20</strong>12<br />

= ×1,000,000 = × 1,000,000 = 10990<br />

So, DPMO is 10990.<br />

3.4.2 Schimdt and Launsby formula [4]<br />

Sigma = 0.8406 + Sqrt (29.37-2.221×ln(DPMO))<br />

Capability= Sigma/3<br />

So, Sigma = 3.7908.<br />

This clearly shows that defect level has come down and sigma level has improved. It is now 3.79. Finally the success<br />

was achieved in reducing the defect level to such an extent. We could have achieved even more but that required<br />

changes in the whole processes, using high quality machines, automatic machines for clamping and packaging<br />

purpose. All these steps will decrease the manual effort and decrease the time taken thus improving the efficiency <strong>of</strong><br />

the process.<br />

3.5 Control phase<br />

The final step in this DMAIC project was to ensure that the proposed improvements should be applied in the<br />

manufacturing process <strong>of</strong> bricks. Further stress should be paid on other improvements as well particularly in the<br />

method <strong>of</strong> Firing. There is a need to understand that new methods can further be improved. Also we should<br />

summarize our key learning’s and involve every worker in suggesting improvements. We should also develop a<br />

Monitoring System. Whenever, the inputs were determined to be out <strong>of</strong> bounds, immediate attention should be given<br />

to correct the situation and bring the process back under control.<br />

4.0 Conclusion<br />

So finally the success was achieved in reducing the defect level and thereby improving the sigma value in. The final<br />

sigma value <strong>of</strong> 3.79 is achieved. However if industries want to retain or improve this sigma value, necessary control<br />

measures have to be taken and proper checks have to be imposed. Quality culture must be developed amongst<br />

employees and proper training must be given to them. A good decision for project generation not only provides<br />

pr<strong>of</strong>its but also increases customer satisfaction. This study aims to investigate the effect <strong>of</strong> applying six sigma tools<br />

in a Brick Kiln industry trying to decrease the scrap rate. This study has two advantages. First is to choose the best<br />

tools that fit that type <strong>of</strong> industry. Second is to encourage similar companions to apply the same methodology.<br />

5.0 References<br />

1. Linderman, K., Schroeder, R., Zaheer, S., Choo, A., (<strong>20</strong>03). “Six Sigma: A goal-theoretic perspective”,<br />

Journal <strong>of</strong> Operations Management, Vol. 21, No. 2, Mar., pp. <strong>19</strong>3-<strong>20</strong>3.<br />

2. Pande, P., Neuman, R., Cavanaugh, R., (<strong>20</strong>00). “The Six Sigma Way: How GE, Motorola, and Other Top<br />

Companies are Honing Their Performance”, McGraw-Hill, New York.<br />

3. Breyfogle, F. W. (<strong>20</strong>03), “Implementing Six Sigma: Smarter Solutions Using Statistical Methods”, Wiley.<br />

4. Schmidt , S.R., and Launsby, R.G., Understanding Industrial Designed Experiments, 4 th ed., Air Academy<br />

Press, Colorado.<br />

922

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