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598<br />

Part Four<br />

Improvement<br />

Source: © Vladimir Repik/Reuters/Corbis<br />

conceived before the days of sophisticated computercontrolled<br />

safety systems. Because of this, the reactor’s<br />

emergency-handling procedures relied heavily on the skill<br />

of the operators. This type of reactor also had a tendency<br />

to run ‘out of control’ when operated at low power. For this<br />

reason, the operating procedures for the reactor strictly prohibited<br />

it being operated below 20 per cent of its maximum<br />

power. It was mainly a combination of circumstance and<br />

human error which caused the failure, however. Ironically,<br />

the events which led up to the disaster were designed to<br />

make the reactor safer. Tests, devised by a specialist team<br />

of engineers, were being carried out to evaluate whether the<br />

emergency core cooling system (ECCS) could be operated<br />

during the ‘free-wheeling’ run-down of the turbine generator,<br />

should an off-site power failure occur. Although this<br />

safety device had been tested before, it had not worked<br />

satisfactorily and new tests of the modified device were to<br />

be carried out with the reactor operating at reduced power<br />

throughout the test period. The tests were scheduled for<br />

the afternoon of Friday, 25 April 1986 and the plant power<br />

reduction began at 1.00 pm. However, just after 2.00 pm,<br />

when the reactor was operating at about half its full power,<br />

the Kiev controller requested that the reactor should continue<br />

supplying the grid with electricity. In fact it was not<br />

released from the grid until 11.10 that night. The reactor<br />

was due to be shut down for its annual maintenance on<br />

the following Tuesday and the Kiev controller’s request<br />

had in effect shrunk the ‘window of opportunity’ available<br />

for the tests.<br />

The following is a chronological account of the hours up<br />

to the disaster, together with an analysis by James Reason,<br />

which was published in the Bulletin of the British Psychological<br />

Society the following year. Significant operator actions<br />

are italicized. These are of two kinds: errors (indicated by<br />

an ‘E’) and procedural violations (marked with a ‘V’).<br />

25 April 1986<br />

1.00 pm Power reduction started with the intention of<br />

achieving 25 per cent power for test conditions.<br />

2.00 pm ECCS disconnected from primary circuit. (This<br />

was part of the test plan.)<br />

2.05 pm Kiev controller asked the unit to continue supplying<br />

grid. The ECCS was not reconnected (V). (This particular<br />

violation is not thought to have contributed materially to the<br />

disaster, but it is indicative of a lax attitude on the part of<br />

the operators toward the observance of safety procedures.)<br />

11.10 pm The unit was released from the grid and continued<br />

power reduction to achieve the 25 per cent power<br />

level planned for the test programme.<br />

26 April 1986<br />

12.28 am Operator seriously undershot the intended power<br />

setting (E). The power dipped to a dangerous one per cent.<br />

(The operator had switched off the ‘auto-pilot’ and had<br />

tried to achieve the desired level by manual control.)<br />

1.00 am After a long struggle, the reactor power was<br />

finally stabilized at 7 per cent – well below the intended<br />

level and well into the low-power danger zone. At this point,<br />

the experiment should have been abandoned, but it was<br />

not (E). This was the most serious mistake (as opposed to<br />

violation): it meant that all subsequent activity would be<br />

conducted within the reactor’s zone of maximum instability.<br />

This was apparently not appreciated by the operators.<br />

1.03 am All eight pumps were started (V). The safety regulations<br />

limited the maximum number of pumps in use at<br />

any one time to six. This showed a profound misunderstanding<br />

of the physics of the reactor. The consequence<br />

was that the increased water flow (and reduced steam<br />

fraction) absorbed more neutrons, causing more control<br />

rods to be withdrawn to sustain even this low level of power.<br />

1.19 am The feedwater flow was increased threefold (V).<br />

The operators appear to have been attempting to cope with<br />

a falling steam-drum pressure and water level. The result<br />

of their actions, however, was to further reduce the amount<br />

of steam passing through the core, causing yet more control<br />

rods to be withdrawn. They also overrode the steamdrum<br />

automatic shut-down (V). The effect of this was to<br />

strip the reactor of one of its automatic safety systems.<br />

1.22 am The shift supervisor requested printout to establish<br />

how many control rods were actually in the core. The<br />

printout indicated only six to eight rods remaining. It was<br />

strictly forbidden to operate the reactor with fewer than<br />

twelve rods. Yet the shift supervisor decided to continue<br />

with the tests (V). This was a fatal decision: the reactor was<br />

thereafter without ‘brakes’.<br />

1.23 am The steam line valves to No 8 turbine generator<br />

were closed (V). The purpose of this was to establish the<br />

conditions necessary for repeated testing, but its consequence<br />

was to disconnect the automatic safety trips. This<br />

was perhaps the most serious violation of all.<br />

1.24 am An attempt was made to ‘scram’ the reactor by<br />

driving in the emergency shut-off rods, but they jammed<br />

within the now-warped tubes.

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