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The Nimrod Review - Official Documents

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<strong>The</strong> <strong>Nimrod</strong> <strong>Review</strong><br />

8.23<br />

154<br />

Again, evident here are the signs of a somewhat ‘closed-loop’ thinking, i.e. the analysis of events in terms of their<br />

perceived frequency, as opposed to in terms of their potential outcome or seriousness, such as to provoke a deeper<br />

safety analysis. This was clearly not just a small fuel leak, confined to the immediate area of the coupling.<br />

(4) December 2000: <strong>Nimrod</strong> XV229 incident – leak from FRS coupling onto hot duct<br />

8.24<br />

8.25<br />

Just three months after the above incident, there was a further incident in December 2000 on XV229. Ground<br />

crew were conducting ground engine runs while attempting to trace leaks in the SCP’s pressure regulating and<br />

shut off valve (PRSOV). To do so, they had removed the insulating muff. During the ground runs, fuel began to<br />

leak from an FRS coupling in the “stbd rib 1 rear spar compartment . As the fuel dropped onto the PRSOV and<br />

associated ducting it began to smoke”. Investigation revealed that fuel was leaking from the FRS coupling on<br />

the No. 6 tank transfer fuel pipe, rib 1, starboard side above the hot air duct. <strong>The</strong> FRS coupling seal was found<br />

to be split and deformed, “presumably due to ageing, thus allowing fuel to leak out”. A Ground Incident Report<br />

was raised10 . In the section for Further Actions/Comments, it was noted:<br />

“Leak attributed to ageing seal and seal has been replaced. However, no trend of ageing<br />

seal related faults apparent at 1st Line or through IRD(F&F) Report. This occurrence<br />

suspected to be isolated incident and EA will monitor for future occurrences. AC has flown<br />

several sorties without related incident and no further action is considered necessary.”<br />

(emphasis added)<br />

In the section for AV(Spey) remarks/Recommendations, it was then noted that:<br />

“FRS couplings are susceptible to leakage if misaligned, fitted incorrectly or overtorqued,<br />

and whilst we have no explicit evidence of these in this particular incident, we do believe<br />

these causes are more likely than ageing. Furthermore, there is evidence on other airframe<br />

types (Harrier) of FRS seals leaking due to causes other than ageing. <strong>The</strong>refore, other than<br />

monitor future arisings for trending [sic], the incident is closed.” (emphasis added)<br />

8.26 In this report, therefore, one sees an awareness of some of the issues that I discuss in Chapter 5, namely the<br />

fact that seals age and that FRS couplings may leak if incorrectly fitted or misaligned. Once again, however,<br />

the incident was treated as an isolated one, without (it would appear) any detailed investigation of any earlier<br />

incidents being made. Nor would it appear that the ‘smoking duct’ (which was admittedly uninsulated at the<br />

time) caused anybody to think more widely about the potential risks posed by fuel dripping from a leaking<br />

coupling onto one of the hot air ducts or perhaps penetrating the insulation.<br />

(5) May 2002: Tornado GR4 ZA599 Incident – coupling fuel leak ignited by bleed air pipe despite<br />

insulation<br />

8.27<br />

8.28<br />

In terms of ignition sequence, the incident most similar to the fire which occurred on XV230, was the loss of a<br />

Tornado GR4A ZA599 on 17 May 2002, as a result of a coupling fuel leak ignited by a bleed-air pipe.<br />

Tornado GR4 ZA599 was flying from RAF Marham on a routine low level flying mission when it suffered multiple<br />

control failures. Fortunately, the crew managed to eject successfully before the aircraft crashed into the River<br />

Humber. <strong>The</strong> Tornado ZA599 Board of Inquiry (Tornado BOI) found that the aircraft had suffered a mechanical<br />

control rod failure as a result of a fuel fire in the spine of the aircraft in Zone 23. <strong>The</strong> fuel source was a fuel leak,<br />

caused by an incorrectly sealed elastomeric ‘O’ ring in a vent line, dripping and pooling onto the spine floor in<br />

Zone 23. <strong>The</strong> ignition source was the bleed-air Hot Intercooler Ejector Pipe, which was insulated with a twopiece<br />

Refrasil jacket which was not liquid or vapour proof. <strong>The</strong> insulation was found to be particularly vulnerable<br />

where there were muffs over bellows attached with spring clips or locking wire. 11 Tests showed the lagging was<br />

impregnated with fuel residues. 12<br />

10 Ground Incident Report KIN/142/00.<br />

11 BOI Report into Tornado ZA599 17 May 2002 incident, paragraph 41(a); and see Annex W: “Interim Evaluation by the Tornado Maintenance<br />

School”, paragraph 21.<br />

12 BOI Report into Tornado ZA599 17 May 2002 incident, Annex T: BAE Systems Report BAE-WME-RP-TOR-CHM-300940, dated September 2002.

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