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The Nimrod Review - Official Documents

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<strong>The</strong> <strong>Nimrod</strong> <strong>Review</strong><br />

28<br />

3.7.10 <strong>The</strong> fire would have considerably weakened the aircraft’s spar and the aircraft’s hydraulic systems would<br />

have begun to fail as hydraulic liquid boiled and pipe unions melted. <strong>The</strong> loss of primary and backup<br />

hydraulic systems and possible fire damage to flying control cables and pulleys, probably led to a<br />

loss of control at some stage during the last 60 seconds of flight. During this period, the No. 7 tank<br />

was probably subjected to a boiling liquid expanding vapour explosion (BLEVE), either as a result of<br />

wing deformation or as internal pressure began to rise to a point at which it ruptured. <strong>The</strong> BLEVE was<br />

probably the fireball reported by the GR7 pilot and Canadian witnesses.<br />

3.7.11 Very shortly afterwards, and at a height of about 700 feet above ground level, the weakened starboard<br />

wing failed, breaking from the aircraft and striking the tail structure. As the remaining aircraft structure<br />

began to roll to the right, the port wing also failed and, shortly thereafter, the tail structure broke from<br />

the aircraft. All four principal elements of the aircraft structure struck the ground within close proximity.<br />

<strong>The</strong> accident was not survivable.<br />

BOI’s Conclusions as to the Probable Physical Causes of the Accident<br />

3.8<br />

3.9<br />

3.10<br />

In summary, therefore, whilst the BOI was unable to determine positively the exact source or causes of the fire<br />

which led to the loss of XV230 and its crew, 13 the BOI found that the following were the most probable physical<br />

causes of the fire and explosion: 14<br />

3.8.1 <strong>The</strong> escape of fuel during AAR, occasioned by an overflow from No. 1 tank, or a leak from the fuel<br />

system (fuel coupling or pipe), led to an accumulation of fuel within the No. 7 Tank Dry Bay. Although of<br />

a lower probability, the fuel leak could have been caused by a hot air leak damaging fuel system seals;<br />

and<br />

3.8.2 <strong>The</strong> ignition of that fuel following contact with an exposed element of the aircraft’s Cross Feed/SCP<br />

duct.<br />

<strong>The</strong> BOI also identified the following as being possible contributory factors to the accident:<br />

3.9.1 <strong>The</strong> age of the <strong>Nimrod</strong> MR2’s non-structural system components;<br />

3.9.2 <strong>The</strong> <strong>Nimrod</strong> MR2 maintenance policy in relation to the fuel and hot air systems;<br />

3.9.3 <strong>The</strong> lack of a fire detection and suppression system within the No. 7 Tank Dry Bay;<br />

3.9.4 <strong>The</strong> fact that the <strong>Nimrod</strong> Safety Case (NSC) did not correctly categorise the potential threat to the<br />

aircraft caused by the co-location of fuel and hot air system components within the No. 7 Tank Dry Bay<br />

(see further below); and<br />

3.9.5 <strong>The</strong> formal incorporation of the AAR capability within the <strong>Nimrod</strong> did not identify the full implications<br />

of successive changes to the fuel system and associated procedures.<br />

<strong>The</strong> BOI further made a number of additional observations, including:<br />

3.10.1 Changes to RAF Kinloss’ management structure as a result of Project Trenchard removed the SO1<br />

engineer (OC Engineering Wing) from the station structure, with the consequence that engineering<br />

personnel were distributed between the station’s two remaining wings under non-specialist leadership<br />

and Queen’s Regulation 640 responsibility was delegated to a squadron leader. Both operational and<br />

engineering witnesses believed that this change had had a negative effect on aircraft availability.<br />

I consider this issue further in Chapter 13.<br />

13 Given that the BOI was unable to investigate the wreckage at the crash site and it proved impossible to recover more than a few small components<br />

from the aircraft.<br />

14 BOI Report, paragraph 60 [2-44 to 2-45].<br />

15 BOI Report, paragraph 61 [2-45].<br />

16 BOI Report, paragraph 64 [2-45 to 2-46].<br />

16<br />

15

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