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The Nimrod Review - Official Documents

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<strong>The</strong> <strong>Nimrod</strong> <strong>Review</strong><br />

52<br />

4.36<br />

This confirms that combustible fluids can gather under the muff; both hydraulic fluid and fuel in this case.<br />

Since the SCP has not been used since September 2006, it is difficult to determine when this incident may have<br />

occurred. Regular maintenance checks of the SCP on the ground were carried out until July 2008 and would<br />

only have used low engine power settings consistent with the results of the chemical analysis. It remains a<br />

possibility that, under the normal operating temperatures of the SCP pipe experienced before September 2006,<br />

the hydraulic fluid could have been ignited, as indeed would fuel. <strong>The</strong> precise sequence of events will never be<br />

known but, in my view, it is powerful corroboration of the BOI’s finding on likely ignition point and proof that<br />

fluids can, and do, enter the SCP elbow muff (see Figures 4.9 and 4.10).<br />

Figure 4.9: XV255 Flexible Muff<br />

Note: the muff shown on the photograph was the item taken off XV255 and shows the<br />

scorching. <strong>The</strong> part is, however, not the correct muff for this bellows and is in fact 6cm<br />

longer then the correct part. Thus, it may give the incorrect impression that the muff is<br />

designed to cover the gap between sections of Refrasil.<br />

Gap<br />

Gap<br />

Deterioration in outer<br />

surface of muff<br />

Blackening caused by 'pyrolysis' of<br />

OX87/OX7<br />

SCP elbow<br />

Gap<br />

Figure 4.10: SCP Expansion bellows/flexible muff (showing deterioration)

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