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Small Decentralized Hydropower Program National ... - Cd3wd.com

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corriente lo llene de pedregullo durante el period0 de<br />

la creciente.<br />

La regla es simplemente suministrar un area de<br />

escape mucho mayor que lo que parezca necesario en<br />

un principio. Se debe dirigir la zanja de la descarga<br />

agua abajo por una corta distancia antes de que se<br />

una a la corriente principal.<br />

Historia de Algunos Casos<br />

Una turbina Francis de 25 kW fu& instalada en un<br />

lugar remoto en un pais de1 norte de Africa para fun-<br />

cionamiento sin ninguna conecci6n a ninguna otra<br />

fuente de generacibn. La unidad fu6 colocada sobre<br />

la corriente, oper6 bien por aproximadamente cinco<br />

meses y entonces una gran tormenta caus6 el creci-<br />

miento de1 agua en la corriente de donde se tomaba<br />

el agua, por medio de un canal de 600 metros a una<br />

antecamara de madera y cafietias de presi6n de<br />

acero, para la turbina. Me encontraba yo en el pais y<br />

me pidieron que inspeccionara la turbina sin d&rseme<br />

descripci6n de1 dtio, ~610 me dijeron que no<br />

funcionaba.<br />

Al llegar a la villa, donde no habia habido luz desdz<br />

varios meses atras, observe que la salida era casi<br />

paralel;l. a! flujo de corriente principal. El canal de<br />

600 metros estaba parcialmente lleno de pedregullo<br />

casi a todo lo largo. La rejilla protectora contra<br />

basura se habia derrumbado dejando paso a una ca-<br />

rnionada de grava que descend% por la ctieria<br />

depresi6n a la turbina. Al pie de la caiietia de<br />

presidjn, un coda de radio largo alimentaba el agua (y<br />

la grava) directamente en la caja de las <strong>com</strong>puertas y<br />

de1 rotor. La mkquina estaba desttida.<br />

Solucih. Rediseiiar la salida a 90 grados, in&alar<br />

las piletas de sedimentaci6n a cada extremo de1<br />

canal, mantene: limpia la rejilla de protecci6n contra<br />

basura y reforzar 10s soportes.<br />

Una turbina vertical a helice de 100 kW habia fun-<br />

cionado bien por aproximadamente cinco ties im-<br />

pulsando a un generador con eje horizontal a trav&<br />

de una caja de engranajes de angulo 3:l. La caja<br />

engranajes habia sufrido una falla. El fabricante<br />

habia suministrado piezas de repuesto para recon-<br />

strucci6n en el campo, pagando el costo. Como una<br />

semana despu& de haber <strong>com</strong>enzado a funcionar, la<br />

caja de engranajes producia ta.1 ruido que el operador<br />

decidid cerrar el sistema.<br />

Al llegar al lugar encontre que la caja de engranaje<br />

habia sufrido dafio que ya no se podia reparar. La<br />

turbina estaba en una caja de presidn de 9 pies de<br />

week after start-up the gear box became so noisy<br />

that the operator shut the system down.<br />

Upon arrival at the site, I found the gear box to<br />

be damaged beyond repair. The turbine was in a<br />

9 foot diameter pressure case with a single side<br />

inlet. The client was a mining <strong>com</strong>pany with<br />

machine-shop facilities. Penstock was 5 feet in<br />

diameter, nearly vertical and supported on con-<br />

crete piers crossed by two 24 inch l-beams on<br />

about 14 foot spans.<br />

I set up dial indicators on the hub of the gear<br />

box, reading on the hub of the turbine. Next I<br />

blocked rotation of the turbine and filled the<br />

penstock and pressure casing. The turbine hub<br />

moved 105 thousandths of an inch with respect<br />

to the gear hub. The entire system lacked rigidity.<br />

Solution. I ordered a thrustit bearing for the<br />

generator and mounted it vertically, installed<br />

Timken roller tail-shaft bearing on turbine shaft<br />

and installed 15G H.P. industrial “Vee-Belt” drive<br />

from spares client had on hand for Ball-Mill<br />

drives. Unit has now been in operation for a little<br />

over three years without further trouble.<br />

A <strong>com</strong>ment: It is probable that this system<br />

col:ld have been stiffened to control the deflec-<br />

tions that were damaging the gear box. The time<br />

element spelled out the solution that was used.<br />

The cause of the damage was the failure to pro-<br />

vide adequated support for the penstock.<br />

The client was a large U.S. paper <strong>com</strong>pany,<br />

engaged in generating his own power with a pair<br />

of vertical shaft Kaplan turbines. During the<br />

period of adequate water, he ran both units and<br />

generated very little steam electricity. During the<br />

summertime, he ran one unit only and shut the<br />

other one down. About three years after start-up,<br />

with one unit running, lightning struck the power<br />

line between the power plant and the paper mill.<br />

Damage was confined to the spider and keys<br />

that attached the umbrella-type generator to the<br />

vertical turbine shaft. The spare unit was running<br />

when I arrived at the site.<br />

Solution. The spider had to be replaced and it<br />

took the rest of the summer. By autumn both<br />

were running and ran throughout the winter.<br />

Calculations made with respect to the failed<br />

spider revealed no design weaknesses. We could<br />

see that the forces generated by the lightning<br />

could reoccur. We re<strong>com</strong>mended that both units<br />

164

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